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MLG19PDSAW Maytag Washer Dryer Combo - Instructions

All Instructions for the MLG19PDSAW
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Rattling sound.
Turned off circuit breaker. Removed two screws at base of front panel with stubby Phillips-head screwdriver. Swung panel up about 30-degrees, and removed panel, disconnecting red and yellow wire to door switch. Removed four sheet metal screws and took off large drum support bracket. Checked drum support rollers and shafts. They were fine. Reset circuit breaker and turned on dryer. Rattling noise still present.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Laurence from Leesburg, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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Gas dryer runs, but no heat.
Unplug the dryer and remove the front panel (two screws at bottom of the panel), being careful of the door switch wires attached to the front panel. Using an ohm meter, I checked the ignitor for continuity and found it was open (should be 50-100 ohms). Make sure to check the solenoids on the gas valve. When the igniter goes bad, it will usually burn out the valve 1 solenoid boost coil (the one with 3 terminals), which was the case with my dryer. The solenoid coils are held in by a bracket with two screws (series 01 dryer) and are easy to remove and replace. Be careful replacing the igniter as the heating element is VERY fragile. Take the time to vacuum out all of the accumulated lint and dust inside the dryer while the front panel is removed, including the lint trap and duct. New igniter and boost/hold solenoid fixed the problem.
Parts Used:
Flat Style Igniter
  • Anthony from Merritt Island, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Would not heat sometimes
Pulled the big front panel by removing two screws near bottom of front and pulling out at bottom until the top pops loose. Vacuumed out all of the dust and checked for loose connections. Ran dryer - igniter would light, but no gas. Checked the two solenoids with a VOM. the one with the two leads would intermittently read Infinity (open). Super simple repair. Remove two screws on solenoid bracket on top of the gas valve, Replace solenoid and plug it back in with the easy push-on connector. NO PROBLEM - all fixed.
Parts Used:
M Series New Style Coil Kit
  • Chris from Laguna Niguel, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Dryer was making awful noise during use
Removed the screws and took the door off then took the front panel off and popped up the top. Then pulled the drum out. Took snap ring pliers and removed rollers and replaced with new rollers then vacuumed all lint from machine and reversed operation to put everything back together. Operation was a total success!
Parts Used:
Drum Support Roller Kit
  • Pam from Aberdeen, WA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Dryer made very loud squealing, screeching noise. (Sometimes Intermittent, sometimes constant)
Note: You may want to consider replacing the 2 Drum Support rollers at this time (while your in there)

1. UNPLUG YOUR DRYER FIRST.

2. Using a phillips head screw driver - Remove 2 screws that secure the dryer door hinges to the frame, Lift door very slightly to unhook hinges and pull out door with hinges attached as straight as possible, set aside. Remove the 2 plastic tabs from the opposing side of the door hinge also secured by screws.

3. Remove the front panel (panel is shaped like a football goal post) by tilting out the top ends of the front panel toward you, then lift up to remove panel from the bottom metal retaining tabs.

4. Remove the 2 hexhead screws from the 2 retaining clips (security hooks) that secure the top
of the dryer closed.

5. Systematically remove the hexhead screws from the rest of the front of "shroud" (it holds (suspends) the drum in place between the front and back of the dryer).

*** I didn't disconnect any wires, I carefully swung out each piece that had wires attached, propped up those parts vertically ensuring no strain on the attached wires. Others may want to disconnect wires to avoid breaking or damaging them.

6. Vacuum out any dust/lint that may be present.

7. Draw a quick diagram of how the underside of the belt is threaded on the idler pulley and motor pully first. Release the tension of the belt from the underside of the drum. The easiest way is to push the idler pulley arm away from the belt and slide off the belt from the idler pulley and motor pulley. Slide the drum out.

8. Remove the hexhead screw from the bottom of the idler arm. Disconnect from retaining spring.

9. You may only need to replace just the Idler Pulley Wheel. I recommend replacing as a "unit" the Idler Pulley Wheel, Idler Arm, Ring-E and Idler Shaft Washer(s) - then you can just swap out the old one for the new one.

10. Reassemble

(When reassembling the belt - place around drum first and slide drum in place. Now from the underside-place (drape) belt around the motor pulley (it will be very loose) Now push the idler pulley arm toward the motor pulley, engage the left side of the belt around the idler pulley and slowly allow idler pulley to increase its tension on the belt) You can test manually by rotating the drum by hand to ensure proper movement.)
Parts Used:
Idler Arm and Shaft Dryer Idler Pulley Wheel & Bearing Idler Pulley Shaft Washer Idler Shaft Retaining Ring
  • Lisa from Trenton, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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Heat Would Not Come On
After replacing all the other fuses and sensors I finally replaced the Radiant Flame Sensor and it is working perfectly.

After replacing the other parts and the heat still not coming on I read somewhere that the Radiant Flame Sensor is a normal closed circuit and when I checked with a meter it was open. I would have saved a lot of time and money if I had read that earlier.
Parts Used:
Dryer Radiant Flame Sensor
  • Lynn from Novi, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
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Replaced two parts in the gas heater assembly
I removed the front panel of the dryer by removing the 2 screw that secure it at the bottom and pulling upward to disconnect the cover at the top. I then removed the two screws that hold the metal cover that secures the 2 elements in place. I disconnected the wire plugs from the 2 elements, removed the 2 elements and replaced them with the new parts making sure to place them in the same positions as before. I then replaced the housing cover and tightened the screws. Then I replaced the front cover of the dryer.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • L R from Carmel, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!

NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Robert from Buffalo, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Dryer wouldn't heat
I removed the front of the dryer by removing the two screws on the bottom of the front panel, disconnected the door switch wires. I removed the connectors from the coils on the gas valve, the heat sensor and the igniter. Loosened the gas line at the valve. I removed the screw holding the gas valve and burner assembly and removed the assembly from the dryer. Remover the screw holding the burner to the valve, and removed the igniter. Replaced the burned and reconnected what I had removed. The reason the burner didn't light was due to the gas deflectors being burned off of the burner, If the igniter, sensor, and coils check out OK , check the front of the burned to besure it is deflecting gas to the igniter
Parts Used:
Burner Tube
  • Clarence from Vienna, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set, Wrench (Adjustable)
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Daughters destroyed door seal with comforter caught in the door...
*** MY REPAIR STORY ***

*** Rule #1: READ THE OTHER STORIES FIRST! ***

The best tip was supplied by the guy that used a piece of good twine/string to help him reconnect the inner seal cable and spring assembly; the whole business of using a buddy to do so is a lot of hooey. Save yourself the aggravation of using your wife, kid or other mechanically-declined individual, and use the string trick. It is still a royal pain, but it is far superior with only one person, using the unbeatable mechanical advantage that the string gives you. I used a piece of good waxed poly twine; I tied it to a convenient hole near the front right side corner of the machine, and then threaded it throught the spring and pulled it with some good pliers in order to stretch the spring enough to re-engage the other loop of the inner seal cable, using needle nose pliers. Of course, it took about four shots to get it right, but I was particularly anal about getting the cable ends in their originally-installed orientation. In retrospect, it ought not make too much of a difference, as long as you keep the spring near the top of the drum and respect the placement of the cable: make sure it is fully in its recess in the seal, all the way 'round. Additionally, pay close attention to the drain hose attachment and outer seal installation; you don't want any more leaks. I have strong fingers so it was a snap, and there are both molded recesses, arrows and "tits" along the seal edges that correspond to the outline of the machine's mating surfaces. Please take the time to push in all the lugs all the way all around in all positions; your floor's dryness is depending on you. As far as the inner seal cable/spring situation goes, be aware that any slight failure to get it right will likely cause a "domino effect" that will necessitate that you to reinstall the seal along its entire periphery, on both inner and outer sides... hold onto that cable, and watch as you tension the spring... it will cause the inner seal to walk off the drum if you aren't paying attention, and you will not be able to recover the perfect position you had at first. In honesty, that is the only "difficult" part of the job. Ensure you've had ample food & drink before you undertake seal replacement ( and not alcoholic drink, either... ) !

As with all jobs of this type, the end was far better than the beginning... the machine doesn't spew water out onto the floor anymore, and helped reinforce my claim to the "most useful" Family Member status! lol My wife was nice to me for almost a week afterwards... your mileage may vary.

PartSelect.com, thank you so much for not only the right part at the right price delivered fast, but also the forum where others could report their repair experiences in order to give a good heads up to those contemplating this repair job. Super site, super business, would definitely use again. A+

Regards,

Glenn Buononato
Parts Used:
Bellow
  • Glenn from New Paltz, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
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Rear Felt seal came out, squealing sound when drying
Turned off gas and unplugged dryer
1) Removed bottom front panel
2) lifted top panel up like a car hood
3) Removed door springs
4) disconnected electrial connections to door unit, removed door unit
5) removed drum, scraped old felt from drum
6) glued new felt with a very strong glue (nanoglue or gorilla glue, same thing), let it dry overnight
7) secured back inside panel, replaced drum and put dryer back together.
Parts Used:
Dryer Drum Felt Seal
  • Matthew from Lombard, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Bad pressure switch on front loading washer allowed water level to exceed proper height leading to water leaking from door seal.
First I sent the local repair man away. I recieved much better advice from this forum. Partselect saved me literally hundreds of dollars. The local repair man was headed in the totally wrong direction.

After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
Parts Used:
Water Level Pressure Switch
  • Paul from Tallahassee, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
17 of 20 people found this instruction helpful.
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The spinner support had sheared off
First, I removed the drum. Removed the spinner support. Removed old seals. Reinstalled new spinner support. Reinstalled pulley and belt. Reinstalled drum. Reinstalled machine covers.
Parts Used:
Spinner Support and Seal Kit
  • Stacie from Las Vegas, NV
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
22 of 35 people found this instruction helpful.
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converted gas dryer to LP
Instructions were great. Very step by step. It could not have been easier. Repair saved me a $100 service call.
Parts Used:
Gas Dryer Conversion Kit - NG to LP
  • Bruce from Rogers, AR
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Wrench (Adjustable)
16 of 18 people found this instruction helpful.
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loud noise inside dryer
After changing all the rollers in the dryer (which didn't fix the problem) I decided to take apart the blower. Sure enough, that was the problem. As the dryer heated up, the damaged wheel would swell and start rubbing the housing. I replaced both and fixed the problem. The repair was pretty easy, since I had taken the dryer apart several times replacing the rollers.
Parts Used:
Blower Wheel Blower Housing
  • Terry from Caruthersville, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
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All Instructions for the MLG19PDSAW
46 - 60 of 914