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MLG2000AWW Maytag Washer Dryer Combo - Instructions

All Instructions for the MLG2000AWW
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Burner would not go on on my Stack Set Dryer
Took out two front Panel screws and removed the panel. Removed Gas solenoid coil holding bracket by removing two phillips head screws. Disconnected the coil leads. and removed the coils. Connected the new coils to the leads and set in place. Replaced the holding bracket and the two screws. Replaced the front cover and the two front cover screws. Piece of Cake!
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Robert from North East, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
16 of 24 people found this instruction helpful.
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drum would not spin and would trip the overload protector
pulled the motor and replaced it and not having any issues since.
Parts Used:
Drive Motor - 60Hz 120V
  • joshua from longmont, CO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
21 of 39 people found this instruction helpful.
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door boot seal was all milldew
Unpluged washer. Removed screws from front and removed door. Removed one more screw on each side and was able to remove front panel, and also lift the top. The boot seal was held in place with a wire and a spring. I unhooked the spring and removed the wire and then removed the old boot seal. I then proceeded to reverse the steps to put it all back together. It took me almost 4 hours. I also used the picture on your web sight to see how things were put together. It really helped a lot.
Parts Used:
Bellow
  • gary from tecumseh, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers
15 of 21 people found this instruction helpful.
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Switch did not turn off dryer when door opened
Switch can be removed from outside of dryer and your video described the repair as having to work from inside dryer. But since wires were still attached to old switch, it could be popped out and wires switched. Since there were three wires on new switch to allow it to turn on and off a circuit, it was useful to check the resistance of the switch compressed or released to be certain I was attaching the two wires to the right two poles of the new switch. But that all required only a couple of minutes. Thank you.
Parts Used:
Door Switch Kit
  • paul from madison, CT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
14 of 18 people found this instruction helpful.
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dryer not heating up
Unscrewed 4 screws,pulled off front of machine.Unscrewed 2 screws holding coils on,unplugged coils,installed new coils,plugged in coils,reinstalled 2 screws for hold down brace.Reinstalled front cover,plugged dryer into outlet(remember to unplugged dryer before working on it).started up,instant heat,works great.thanks Partselect for helping me out!!!
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Richard from New Windsor, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
12 of 14 people found this instruction helpful.
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The dryer was not fully drying
After replaceing several parts including the thermostats the last part I replaced the coils were the defective part. I originally metered out the themostats and they appeared to be okay but since this was my first time I thought I might have been mistaken. It turns out the last part I thought it could be was the part that was defective. I will say that it is very simple to replace any of the parts involved. The hardest part was trying to open the dryer itself. But after having to do it 3 times, I'm now a pro. I also replaced the drum belt and since I had it open I also replaced the belf idler with a newer modified idler rolller.

Putting the belt back on is easy, but it helps to view the video or a picture to understand how the belt goes around it.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Michael from Chicago, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
12 of 14 people found this instruction helpful.
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The Dryer would not get hot.
I removed the two screws holding the access panel, and removed the access panel. Then removed the lower air duct. I then checked the burner, The solenoid was not opeing the valve for the gas. I order the coils, in two day I had the coils and installed them. The dryer is working great.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Jerry from Bradenton, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
14 of 20 people found this instruction helpful.
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Washer would not drain
Since the machine would not drain, I suspected the drain pump. A friend in appliance repair tested that for me and it was good. All one has to do with that is hook a test line to the pump with 120 volts and if it runs it is good. He then told me to see it the mother board which is located in the right upper area above the dryer drum had a burned place at a resistor and to note if the door would not lock. I checked this and the circuit board was not damaged and the wax motor which locks the door was working OK. (This unit is a combo stack dryer and washer) I then suspected the timer because my wife told me that it had been making a grinding noise. The timer was replaced by the one you sent me and it solved the problem. ( My friend really did not want to work on this machine since he had replaced the inner drum and bearing about six months ago and it took all day)Thanks a bunch. The timer came in one day from the time of order.
Parts Used:
Washer Timer
  • William from Jennings, FL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench set
13 of 17 people found this instruction helpful.
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Bad Seal Allowed Water to Damage Bearings, makes loud noise in spin
I followed the extensive instructions others had posted on this site about the need to replace the "non-replaceable" bearings. The hard part is getting the old bearings out of the outer tub as they were very corroded. I left the outer tub in the machine and after attempting to beat them out unsuccessfully, I resorted to using a Dremel tool with a small grinding disc on the end to cut the bearings apart, first cutting through the center and removing the ball bearings, then cutting through the outer rim and edge being careful not to cut to deeply, once the bearings were weakened, they came out pretty easily. Installing the new bearings and putting the machine back together was pretty easy. The machine works like new, so for me it was well worth it, thanks to everyone who shared their experiences so I felt comfortable giving it a try!!
Parts Used:
Lip Seal Kit
  • William from New Smyrna Beach, FL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
13 of 17 people found this instruction helpful.
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Dryer runs, but no heat
Removed screws in hinges and on opposite side inside the door to remove the front panel.

You can put the door back on at this point to run the dryer with the burner exposed. At this point I could tell that the igniter was working and the gas valve would occasionally work so that burner would fire. The valve only seemed to work when everything was completely cooled down. I first replaced only the solenoid coils on top of the valve, this did not fix the problem. When I replaced the entire valve the problem was fixed.

Replacing the valve is easy.

1) Unplug dryer from wall outlet
2) Turn off gas supply cutoff valve
3) Remove door and front panel
4) Unplug wires from solenoid coil terminals. There are two coils on top of the valve body.
5) Remove gas line from valve body.
6) Remove two screws which secure the bracket holding the valve body and burner nozzle to the bottom of the dryer cabinet.
7) Remove two screws which secure the valve to the bracket.
8) Reverse the procedure for installation of new valve.
Parts Used:
Gas Valve with Coils
  • doug from dallas, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Wrench (Adjustable)
13 of 17 people found this instruction helpful.
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drum support roller was squeaking
My 11 year old grandson and I did the repair together. He had a blast and I did too. First we removed a bunch of screws that got us no closer to getting the machine apart than when we started. Then I remembered from the last time I had the machine apart that there are two screws just below the door, angled as not to be visable unless you know where to look. Once we removed those the from came off. We removed the wires for the door light and heat sensor, remembering the order of the wires for later reinstallation. Then we undid the bolts holding down the top. Once the top was removed we took off the belt and removed the drum. We used the retainer pliers to remove the retainer ring from the first roller. We removed the roller and also the shaft as this roller was the noise maker and the shaft was not in reusable condition. We installed a new shaft, roller washer, roller, another roller washer and then the retainer ring. We repeated the same process on the other roller, although we did not replace the shaft as it was in good condition. It turned out I did not need to order the shaft washers as the rollers came with washers. Oh well, its not a good job unless you have parts left over when you are done. Once we replaced the rollers we commenced reinstallation. But first we had to google for diagram of the proper belt installation, which we found and that got the drum and belt installed properly. Thankd god for the internet. Once we had the drum installed we put the machine back together in the opposite order we took it apart. An operational test showed we did the job right, no more squeaking. The only injury was my grandson cut his thumb right after I gave him the speech about watching where your hand is going to end up when that bolt breaks free. It broke loose and into the metal bracket went his thumb. Oh well it was a good lesson and it was not a bad cut. All in all a good repair.
Parts Used:
Roller Shaft Dryer Retaining Ring Roller Shaft Hex Nut Drum Roller Shaft Washer Drum Support Roller Kit
  • Kevin from San Diego, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
12 of 14 people found this instruction helpful.
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The moister sensor broke away from it's two fasteners inside the dryer drum.
Unscrewed the two fasteners, rerouted one wire using a wire coat hanger, plugged in the new moisture sensor to the two wires and fastened the the sensor in place using the two existing screws.
Parts Used:
Moisture Sensor
  • David from Preston, CT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
14 of 20 people found this instruction helpful.
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bearing replacement
I haven't finished the job yet. I was very surprised and very happy with how fast PartSelect got my part to me. I ordered a lip seal kit (maytag neptune bearing replacement) in the morning, and the very next day it arrived at my door. I'm very impressed. I have everything cleaned up and ready for the new parts. I just have to finish.

Thanks for the speedy service. I'll be highly recommending PartSelect.

Frank
Parts Used:
Lip Seal Kit
  • Frank from Streator, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Socket set
16 of 27 people found this instruction helpful.
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Failed bearings cause by a failed lip seal
First of all, let me say that the Lip Seal Kit was delivered the next day after my order and that I was encourged to attempt the repair by the owners repair procedure response. The lip seal in my machine must have failed along time ago as I have been living with noisy bearings for at least the last twelve months. Disassembly of the machine was straight forward following the Part Select instructions. The lip seal was so disintegrated it hard to tell what originally looked like. Lots of rust and gunk in lip seal area. After removing the snap ring behind the rear bearing I was able to drive out the rear bearing using a brass 3/4" drift pin and a two# hammer. I than attemped to remove the front bearing using a 1 1/2" steel pipe that matched up to the inner race of the front bearing and my trusty hammer. Nothing I did could budge that bearing. Since the outer tube is suspended by springs and struts I decided that lot of hammer energy is absored by springs and my best solution was to remove the outer tub. I then used a couple pieces of U channel steel(this could be steel pipe or some 2X4's) that were longer than the depth of the tub and positioned them to contact metal bearing tub insert. These supports were mounted in small Workmate vise setting on the garage floor and using the 1 1/2" steel pipe I drove the inside bearing out. After some general clean up I picked up some bearings at the local distributor for $42.00. Re-assembly takes a little planning as you need to hold the steel insert betwwen the bearings and keep it lined up in the bore. I think the best way is to install the rear bearing first and install the snap ring. I then put the steel ring in place and held it with cardboard insert from a paper towel roll. The cardboard roll was cut about 2 1/2" long and cut lenght wise to insert though the rear bearing and held in place with tape. The front bearing was then tapped into place followed by the lip seal. Note that if you install the front bearing first and seat it all the way in, the rear bearing will contact the steel insert and not allow enough room to get the snap ring in place. When I was done I didn't have any parts leftover and thru six washing machine loads peace and quiet has returned to my house. Hope it last. Note: If you elect to remove the outer tub you might want to take some pictures so you can see how it all is supposed to look before you close the hood.
Parts Used:
Lip Seal Kit
  • Thomas from Olathe, KS
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
12 of 15 people found this instruction helpful.
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Bearings making noise.
If you are using the newer style seal be sure the taper part of the seal is toward the front of the machine. Installing it backward will ruin the seal and burn up the motor and or controller. The seal installation tool will fit on the side oppsite the taper. It will require a helper to hold the drum support while torquing the nut on the pulley. Better instruction would help too.
Parts Used:
Outer Tub with Bearing
  • James from Greer, SC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
11 of 12 people found this instruction helpful.
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All Instructions for the MLG2000AWW
91 - 105 of 1162