MLG19PRDWW Maytag Washer Dryer Combo - Instructions
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drum support roller was squeaking
My 11 year old grandson and I did the repair together. He had a blast and I did too. First we removed a bunch of screws that got us no closer to getting the machine apart than when we started. Then I remembered from the last time I had the machine apart that there are two screws just below the door, angled as not to be visable unless you know where to look. Once we removed those the from came off. We removed the wires for the door light and heat sensor, remembering the order of the wires for later reinstallation. Then we undid the bolts holding down the top. Once the top was removed we took off the belt and removed the drum. We used the retainer pliers to remove the retainer ring from the first roller. We removed the roller and also the shaft as this roller was the noise maker and the shaft was not in reusable condition. We installed a new shaft, roller washer, roller, another roller washer and then the retainer ring. We repeated the same process on the other roller, although we did not replace the shaft as it was in good condition. It turned out I did not need to order the shaft washers as the rollers came with washers. Oh well, its not a good job unless you have parts left over when you are done. Once we replaced the rollers we commenced reinstallation. But first we had to google for diagram of the proper belt installation, which we found and that got the drum and belt installed properly. Thankd god for the internet. Once we had the drum installed we put the machine back together in the opposite order we took it apart. An operational test showed we did the job right, no more squeaking. The only injury was my grandson cut his thumb right after I gave him the speech about watching where your hand is going to end up when that bolt breaks free. It broke loose and into the metal bracket went his thumb. Oh well it was a good lesson and it was not a bad cut. All in all a good repair.
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Kevin from San Diego, CA
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Socket set
12 of 14 people
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Bearings making noise.
If you are using the newer style seal be sure the taper part of the seal is toward the front of the machine. Installing it backward will ruin the seal and burn up the motor and or controller. The seal installation tool will fit on the side oppsite the taper. It will require a helper to hold the drum support while torquing the nut on the pulley. Better instruction would help too.
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James from Greer, SC
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Pliers, Screw drivers, Socket set
11 of 12 people
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bearing replacement
I haven't finished the job yet. I was very surprised and very happy with how fast PartSelect got my part to me. I ordered a lip seal kit (maytag neptune bearing replacement) in the morning, and the very next day it arrived at my door. I'm very impressed. I have everything cleaned up and ready for the new parts. I just have to finish.
Thanks for the speedy service. I'll be highly recommending PartSelect.
Frank
Thanks for the speedy service. I'll be highly recommending PartSelect.
Frank
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Frank from Streator, IL
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Socket set
16 of 27 people
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Failed bearings cause by a failed lip seal
First of all, let me say that the Lip Seal Kit was delivered the next day after my order and that I was encourged to attempt the repair by the owners repair procedure response. The lip seal in my machine must have failed along time ago as I have been living with noisy bearings for at least the last twelve months. Disassembly of the machine was straight forward following the Part Select instructions. The lip seal was so disintegrated it hard to tell what originally looked like. Lots of rust and gunk in lip seal area. After removing the snap ring behind the rear bearing I was able to drive out the rear bearing using a brass 3/4" drift pin and a two# hammer. I than attemped to remove the front bearing using a 1 1/2" steel pipe that matched up to the inner race of the front bearing and my trusty hammer. Nothing I did could budge that bearing. Since the outer tube is suspended by springs and struts I decided that lot of hammer energy is absored by springs and my best solution was to remove the outer tub. I then used a couple pieces of U channel steel(this could be steel pipe or some 2X4's) that were longer than the depth of the tub and positioned them to contact metal bearing tub insert. These supports were mounted in small Workmate vise setting on the garage floor and using the 1 1/2" steel pipe I drove the inside bearing out. After some general clean up I picked up some bearings at the local distributor for $42.00. Re-assembly takes a little planning as you need to hold the steel insert betwwen the bearings and keep it lined up in the bore. I think the best way is to install the rear bearing first and install the snap ring. I then put the steel ring in place and held it with cardboard insert from a paper towel roll. The cardboard roll was cut about 2 1/2" long and cut lenght wise to insert though the rear bearing and held in place with tape. The front bearing was then tapped into place followed by the lip seal. Note that if you install the front bearing first and seat it all the way in, the rear bearing will contact the steel insert and not allow enough room to get the snap ring in place. When I was done I didn't have any parts leftover and thru six washing machine loads peace and quiet has returned to my house. Hope it last. Note: If you elect to remove the outer tub you might want to take some pictures so you can see how it all is supposed to look before you close the hood.
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Thomas from Olathe, KS
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Difficulty Level:Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
12 of 15 people
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washer would not drain water
my husband took the old part off. order the new part thru your company...3 days later the part came in. then he reattached thee part to the hoses with the champs and we said alittle pray and i had my washer back
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deb from new madison, OH
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Difficulty Level:A Bit Difficult
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Wrench (Adjustable)
13 of 19 people
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One of the Baffles came loose.
I took out screws holding top to dryer & raised the top & proped it up to gain access to inside of the dryeeer drum. I then inatalled the new baffle & secured it with 2 screws. It would have been better if the part came with new screws.It was hard to determine which was the right screws for this application.
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Robert from Milford, OH
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
12 of 16 people
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Drive belt sqeaked and contiued to roll off the drum.
Removed washer back panel (after unplugging unit). Installed new belt. Reinstalled back panel. Belt wAs very tight getting it to roll onto the drum.
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Douglas from Marion, IN
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
13 of 19 people
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Dryer door latch broken, using duct tape every time to dry clothes.
Piece of cake. Used flat screwdriver to pry out female part on cabinet side, same with the male part on door. Every new replacement part was tight and operated like new. Thanks Part Select, you'll be forever on my list of online parts buying.
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Scott from Palm Bay, FL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
10 of 11 people
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
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Jim from Foothill Ranch, CA
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
10 of 12 people
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Pump would not pump water from washer drum
It was very easy to do. I took the back cover off. I dissconected two hoses. disconnected one wire. removed a small plastic bag (cover over wires). turned the pump 1/4 turn.and reversed this process with the new pump. It took me 15 minutes to remove and replace. Put the washer thru a cycle and it worked!
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David from Watervliet, MI
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Screw drivers
14 of 24 people
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.
The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.
I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.
I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
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Roger from Westminster, SC
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Difficulty Level:Very Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers
12 of 18 people
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High Pitch Noise During Spin Cycle The Seal Failed Causing The Bearing To Fail Also
First I removed front and rear covers and the dispenser screws. If you are carefull you can fold the front cover back and lay it on top of the washer so that you do not have to unplug all the wires. Remove the clips on the front of the outer drum with a small flat blade screwdriver and set aside. Go to the back and roll the belt off the pulley. Remove bolt and snap ring and the pulley should pull toward you off of the shaft. This is plastic be carefull. The inner drum will now pull out thru the front of the machine. Now read the directions again and again about the seal because you have to replace exactly what you take out. This is my only complaint with the directions there needs to be a picture and not an illustration of the placement of the sael and the spacer in my case.
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tommy from madisonville, KY
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Socket set
9 of 10 people
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Broken door strike
Removed one screw and took out old broken door strike, replaced with new door strke and put screw back in. Only took two three days to get the part. The dryer is as good as new!
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Carl from Livermore, CA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
10 of 13 people
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Short Baffle in dryer drum was broke off
This was fairly easy, I have had the dryer front off before. Unplug dryer from electrical outlet. Pull dryer away from wall. Remove the dryer door, open dryer door there are 2 phillips screws on dryer door hing, remove these crews then lift gently and remove door, across from these screws, where dryer door closes into face cover of dryer remove 2 more phillips screws. From top of face cover, pull out front of face cover and lift to remove face cover of dryer. On each side of dryer on the front, after removing the front cover is a 5/16 bolt, remove these and pull off retaining bracket with a twisting motion. You now can lift the top of the dryer up. You can now see the barrel drum. Rotate barrel by hand so the broken baffle is on top. Remove two 5/16 bolts, and replace new baffle in place. Reassemble in reverse order of disassemble.
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Wade from Lovell, WY
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers, Socket set
8 of 8 people
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No heat in dryer
Took off the lower front panel, removed duct piece from filter to blower fan, removed two screws and two wires to thermostat in exhaust ducting, then replaced thermostat with new one. Very easy job and everything worked like new when I reassembled it.
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Noah from Maiden, NC
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Wrench (Adjustable)
10 of 14 people
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