MLG19PRDWW Maytag Washer Dryer Combo - Instructions
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Bad pressure switch on front loading washer allowed water level to exceed proper height leading to water leaking from door seal.
First I sent the local repair man away. I recieved much better advice from this forum. Partselect saved me literally hundreds of dollars. The local repair man was headed in the totally wrong direction.
After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
Parts Used:
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Paul from Tallahassee, FL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
17 of 20 people
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converted gas dryer to LP
Instructions were great. Very step by step. It could not have been easier. Repair saved me a $100 service call.
Parts Used:
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Bruce from Rogers, AR
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Wrench (Adjustable)
16 of 18 people
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Washer would not drain
Starting out I found the code that the washer was showing,ND, Meaning no drain so I read up on and people where saying that the pump had a blockage in it, so I took the back of the washer to gain acess to the pump, I took the drain hose off to look in side to see if there was a problem there was nothing in the pump itself so I started to remove the pump I undid the wiring harness to find the problem, the red wire to the pump had burned in the harness order the part from part select and 30 minutes later my wife was doing laundry again..........Thanks partselect for the fast shipping and quality parts very easy repair.
Parts Used:
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Scott from Sedalia, MO
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers
18 of 24 people
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Bearings making loud rough noise
Thanks to all the others who gave detailed information I was able to replace the front & rear bearings and front seal. I must say it was a time comsuming job but at least I am alot clearer on the quality of clothes washing machines. I do believe I could give a manufacturer / designer some design points after working on this Maytag Neptune. I was able to knock out the bearing shaft that held the stainless perforated tumbler inside the plastic tub/drum by using a #3 LB hammer I reinstalled the old screw in the shaft which held the plastic pully on because this would keep the end of the shaft from being damaged. After several blows it started moving I was afraid I might damage the plastic drum but fortunately no damage was done to it. After removing the stainless steel perforated tumbler here is where it really got interesting. The Hub that held the old seal was shot! pretty much deteorated from corosion it seems. Here is where I could significantly help a manufactured/designer out The bearing/seal hub should have been made out of stainless instead of Pot metal/ aluminum or whatever they made it from. After much cleaning with a small wire brush and vacuming all the debree out of the Tub I didn't have much hub left to install the new seal. Also the three armed Spinner was very coroaded it attaches to the back of the stainless tumbler I removed it from the stainless tumbler and wire brushed it the back side was full of crud, it looked like left over washing powder or soap and Corosion debree it was a job just cleaning it up. I pressed on and on though replacing both bearings front and rear. Thanks to another person who explained the easy way to remove the bearings and race I was able to do so without removing the Drum/Tub as others stated they had to do. The Dremmel and a few Cutter blades did the trick I cut a wide V notch in the bearings and the bearings fell out I then cut through the bearing race being careful not to cut too deeply although if you did slightly cut beyond the race it really wouldn't matter because the front seal will keep it from leaking anyway. Anyway when I cut through the race it made a ping sound and the race pulled away and fell right out of the HuB. The front & rear bearings a definately serviceable and it doesn't have to be a beat/bang ordeal. after cleaning up the hub I tapped the new bearings in place and discarded the metal spacer that went inside the middle of hub. I then brainstormed on how I could install the new Lip Seal upgrade and then it dawned on me that since the inner Hub that holds the seal was so far gone and only enough left to barely hold the new seal in I remembered the ole saying Don't Discard just use JB Stick or JB Quick I used JB Stick to fill in around the new seal because it is supposed to bond to metal and it did just that I pressed the putty in quickly before it hardened bringing it out even with the plastic drum where the origional hub should have been and made the repair to the deteriorated Hub so that the Seal would stay in place it Worked! This Maytag Neptune was given to me by my mother in-law she did not want to wait on the repair after I tried to previously repair the problem with it I just did not delv deeply enough into the problem with this washingmachine at first. I previously removed both Pumps thinking they were not pumping all the water out because the Towels especially were staying soaked. Both the pumps were nasty with alot of debree inside of them now I know that because of the deteriorated Seal Hub on the inside had done the dirty work. The Pumps can be easily taken apart only a few screws and the plastic impeller can be gently pried off also that is where I found alot of particles from the deteoriated Seal Hub I then reinstalled the pumps and they worked fine pumped out the water. Then that is when I noticed it wasn't cycling properly also Ha Ha I thought to myself what else could possibly be wrong with this washing machine? Thanks to Parts Select site I wa
Parts Used:
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Gregory from El Dorado, AR
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Screw drivers, Socket set, Wrench (Adjustable)
17 of 22 people
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Dryer wouldn't start
We tried replacing the door switch first, still didn't start. Next we tried the thermal fuse and it turned on and has worked ever since.
Parts Used:
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SALLY from ANAHEIM, CA
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Pliers, Screw drivers
16 of 19 people
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Time clock not moving .Not enough heat
Opened front panel .Tested both coils on gas valve.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
Parts Used:
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PHILIP from LONG ISLAND CITY, NY
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Pliers, Screw drivers
16 of 21 people
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broken clip for door latch
popped out old female clasp on dryer itself with screwdriver, undid 2 screws on dryer door and door handle with phillips screwdriver, popped in new male clasp part, put door knob back on and put the two screws back in door and it was all set to go. Less than 15 minutes to do. Better than new and wife is happy. No more duct tape holding door closed now.
Parts Used:
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Shawn from Dover, NH
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
14 of 15 people
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Front bearings totally destroyed rear bearings rusted out
I found your site where other people worked on their washers . I removed the front & rear panels. at the front I found that removing the rubber tub seal was easy, then I removed the 3 agitaters that cover the nuts that hold the tub to the support drive shaft ,I saved the plastic shims nuts & washers then removed the tub,I removed the drive wheel, I put the bolt & washers back in the shaft end & knocked it out with a 1lb hammer.I removed the motor and all the hoses also the front & rear WeightsI left the switches connected to the wires, for everything I removed including screws I taped them all to the parts that they camefrom .Then I knocked out the rear bearing with a 8" long 1/2'dia.piece of steel rod taking care to drive evenly around the circomference of the bearing. the front bearing was in 2 pieces with the bearings in a pile inside the hub because of the spacer between the bearings there was not a lot of bearing to hit but eventually it came out I saved the spacer & the rear bearing clip & cleaned them up for reuse.The face of the crap metal insert was badly corroded ,I cleaned it and all surfaces inside the hub with a wire brush in my drillmotor I found bearings at an industrial store and found NO problem matching the old bearings I ordered the lipseal kit from Part select It came with 2 seals & dubious instrutions I found the revised seal did not fit my support shaft but the other one did ,it comes in 2 parts that are stuck together with grease pry them apart with e small screw driver. I then tapped the new bearings in rear first then the spacer. then the front bearing I tapped it in enough to get it started then I inserted a cardboard toilet roll center folded enough to go in through the spacer & the rear bearing this lined up the parts so the shaft will go throughafter the bearings & new seal were in I used a marine silicon to put over the corroded face & made shure that it snugged up to the seal ,sealing it good I let it set for 24 hrs Then I putthe shaft back onto the tub put the agataters back on, then put the outer shell with the new bearings back in place connected the hoses, the weights, the switches, the wire clips,the motor,hooked up the springs ,inserted the tub, put the drive wheel back on the shaft then the belt , then put all the front panels back and IT ALL WORKED. total cost $36.00 for bearings $53.00 for the seal kit so about $90.00 total & two weeks at about a couple of hours a day .shure beats $650.00 + $300.00 at a repair facility . GOOD LUCK .IAN
Parts Used:
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john from richland, MI
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Pliers, Screw drivers, Socket set, Wrench set
14 of 17 people
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Burner would not go on on my Stack Set Dryer
Took out two front Panel screws and removed the panel. Removed Gas solenoid coil holding bracket by removing two phillips head screws. Disconnected the coil leads. and removed the coils. Connected the new coils to the leads and set in place. Replaced the holding bracket and the two screws. Replaced the front cover and the two front cover screws. Piece of Cake!
Parts Used:
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Robert from North East, PA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
16 of 24 people
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drum would not spin and would trip the overload protector
pulled the motor and replaced it and not having any issues since.
Parts Used:
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joshua from longmont, CO
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Screw drivers, Socket set
21 of 39 people
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Switch did not turn off dryer when door opened
Switch can be removed from outside of dryer and your video described the repair as having to work from inside dryer. But since wires were still attached to old switch, it could be popped out and wires switched. Since there were three wires on new switch to allow it to turn on and off a circuit, it was useful to check the resistance of the switch compressed or released to be certain I was attaching the two wires to the right two poles of the new switch. But that all required only a couple of minutes. Thank you.
Parts Used:
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paul from madison, CT
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
14 of 18 people
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dryer not heating up
Unscrewed 4 screws,pulled off front of machine.Unscrewed 2 screws holding coils on,unplugged coils,installed new coils,plugged in coils,reinstalled 2 screws for hold down brace.Reinstalled front cover,plugged dryer into outlet(remember to unplugged dryer before working on it).started up,instant heat,works great.thanks Partselect for helping me out!!!
Parts Used:
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Richard from New Windsor, NY
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
12 of 14 people
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Bad Seal Allowed Water to Damage Bearings, makes loud noise in spin
I followed the extensive instructions others had posted on this site about the need to replace the "non-replaceable" bearings. The hard part is getting the old bearings out of the outer tub as they were very corroded. I left the outer tub in the machine and after attempting to beat them out unsuccessfully, I resorted to using a Dremel tool with a small grinding disc on the end to cut the bearings apart, first cutting through the center and removing the ball bearings, then cutting through the outer rim and edge being careful not to cut to deeply, once the bearings were weakened, they came out pretty easily. Installing the new bearings and putting the machine back together was pretty easy. The machine works like new, so for me it was well worth it, thanks to everyone who shared their experiences so I felt comfortable giving it a try!!
Parts Used:
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William from New Smyrna Beach, FL
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
13 of 17 people
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The Dryer would not get hot.
I removed the two screws holding the access panel, and removed the access panel. Then removed the lower air duct. I then checked the burner, The solenoid was not opeing the valve for the gas. I order the coils, in two day I had the coils and installed them. The dryer is working great.
Parts Used:
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Jerry from Bradenton, FL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver
14 of 20 people
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The dryer was not fully drying
After replaceing several parts including the thermostats the last part I replaced the coils were the defective part. I originally metered out the themostats and they appeared to be okay but since this was my first time I thought I might have been mistaken. It turns out the last part I thought it could be was the part that was defective. I will say that it is very simple to replace any of the parts involved. The hardest part was trying to open the dryer itself. But after having to do it 3 times, I'm now a pro. I also replaced the drum belt and since I had it open I also replaced the belf idler with a newer modified idler rolller.
Putting the belt back on is easy, but it helps to view the video or a picture to understand how the belt goes around it.
Putting the belt back on is easy, but it helps to view the video or a picture to understand how the belt goes around it.
Parts Used:
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Michael from Chicago, IL
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers, Socket set
12 of 14 people
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