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MLE20PDCGW0 Maytag Washer Dryer Combo - Instructions

All Instructions for the MLE20PDCGW0
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Spring balanced tub violent shake on spin
Washer was on a 13 inch high platform I built for front.load Heat washer and dryer. Removed 3.screws from bottom of front panel and had access to all 4 shocks..front and rear. All shocks were unattachedeither at base or on tub. Easy to install all 3 from front without moving Mach. I figured if 1 or 2 shocks failed the violent.movement broke the other 2. Purrs like.a.kitten now. No bearing.or spring.damage.
Parts Used:
Shock Absorber
  • Paul from TARPON SPGS, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
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Screen on the hot air vent disintegrated
It is odd that this part needed replacement but I am in an area near the Atlantic ocean in a vacation house which is vacant most of the year. The exhaust vent probably brings excessive moisture down to the dryer in the basement. The screen you can see at the inside back of the tumbler (where the heated air enters) rotten out, pieces fell inside and there was danger of something falling in and catching fire. I found no useful source for information (including YouTube) as this part is most easily replaced from the rear of the dryer and the available info was about repairing the heating element, the circuit board, or the exhaust venting pieces which is done from the front.

The bottom line is that the back removes easily. You should:
1. unplug and remove the exhaust shoot
2. remove the top per YouTube or other source
3. take off the back panel over the electrical connections and unscrew the ground; tuck it inside. Don't undo any electrical connections except the ground
4. take off the screws holding the back on (8-9, one is hidden above the exhaust vent) and pull it out of the way; you then have compete access to the "DUCT-AIR" part
4. undo the clip that holds the vent tube (from the heating element) to the part
5. remove the screws that hold the part to the inside back (3?) and push it out of the way
6. remove the clips and remove the old part
7. reassemble in reverse order

I'm over 70 so I took lots of time and breaks but was still done in under two hours. The 2 clips holding the heater element tube to the part were badly rusted and should have been replaced but I made do with the old ones.
Parts Used:
DUCT-AIR
  • Thomas from Edgartown, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
3 of 3 people found this instruction helpful.
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Broken Drum Belt
Just like the video, just followed the video
Thanks,
Parts Used:
Dryer Drum Seal with Adhesive
  • Garry from Garland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
3 of 3 people found this instruction helpful.
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Dryer drum turned hard because rollers were worn
Remove top, front and drum. Top is removed by sliding a putty knife under the front corners and pushing the tabs back. Front is held with screws. Disconnect two electrical connectors. Rollers are easily accessible and changed.
Parts Used:
Dryer Drum Support Roller
  • Paul from STONE CREEK, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
3 of 3 people found this instruction helpful.
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dryer would not work .
Took the old parts out and installed the new parts in , everything that you sent fit perfect!!!!!
Parts Used:
Burner Tube Dryer Radiant Flame Sensor Igniter Kit
  • Tom from MEARS, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set
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YouTube video dated 9/28/2015
How to repair E1 error/fault on Whirlpool Duet dryer model GEW9200LW0 please watch that video very helpful.
Parts Used:
Thermostat, Internal-Bias
  • Madeline from PANA, IL
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable), Wrench set
3 of 3 people found this instruction helpful.
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Dryer would shut off mid way through cycle and give an E1 error code
After turning off the power to the dryer I removed two screws to the bottom front panel and droped it out of the way. I remved three screws hloding the lint screen in place just for better axcess to the element. I then removed the two wires attached to the element and then the two screws holding the element in place. I put everything back together in reverse. I also took the time to clean any dust and lint out.
Parts Used:
Thermostat, Internal-Bias
  • Dwayne from Bainbridge, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Socket set
5 of 9 people found this instruction helpful.
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No heat
I had two dryers, one was gas and the other was electric. The electric stopped heating. So I rolled out the gas dryer, but it was setup for natural gas and at this location, I only have propane. So I changed the jets to work with propane, in the process I broke the igniter, so I replaced that and that made the propane one work. Armed with the knowledge from that job, I took the electric dryer apart located the thermostat and replaced that and low and behold I have two working dryers. One for now and one for an emergency. I only have four screws left over!!!! Jim Cooke
Parts Used:
Igniter Kit
  • James from Randsburg, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
4 of 7 people found this instruction helpful.
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Loud squeaking noise
Replaced the most worn drum wheel any lubed the belt tension arm pulley. The noise didn't go completely away. There are 4 drum wheels. I need to order 3 more wheels and the tension arm now.
Parts Used:
Dryer Drum Support Roller
  • Steven from WICHITA, KS
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers
3 of 4 people found this instruction helpful.
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Part broken in half
Remove screws, dryer sensor on screen. Put sensor back in place. Secure with screws. The way you take it off go in reverse.
Parts Used:
Outlet Screen Door Grille Screw - 10-16 x 1
  • Sean from ROCK HILL, SC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
3 of 4 people found this instruction helpful.
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Counter weight flew apart
Three 1/2 bolts tighten as required
Parts Used:
Counterwgt
  • Mark from BENTON, AR
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Socket set
2 of 2 people found this instruction helpful.
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Old. Original heat seal was deteriorated and peeling off. Streaks were getting on the clothes.
Removed the front panel, removed the tub and removed the old seal. Tub seal area was scraped, sanded and wiped with acetone to ensure a clean. Bonding surface. Applied adhesive with and acid brush to get a consistent adhesive layer without getting too much in any one place. Seal was a bit smaller than the tub circumference so it had to be stretch to fit. While the adhesive was curing , I took the time to clean the contact surfaces and vacuum the lint from inside the cabinet. Reinstalled the tub, drive belt and front panel.
Parts Used:
Dryer Drum Seal with Adhesive
  • Lawrence from ARITON, AL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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Washer wouldn't fill!!! Water temp sensor with rubber seal replaced. Happy to say Washer up and running Thank You
very easy repair watched videos to diagnosed problem. Removed old sensor and rubber seal replaced with new.
Parts Used:
SEAL
  • Sue from N PROVIDENCE, RI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
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Torn tub seal causing major water leak.
Removed top of washer. Removed top front panel. Removed old front panel clamp. Removed front door panel. Removed old tub clamp. Then removed torn tub seal. Installed new tub seal. Needed two sets of hands to install new tub seal. Pretty tight installing the new tub seal around drum lip. Might be a good idea to heat up or let your new tub seal soak in water prior to installation. Once tub seal was installed, I installed new tub clamp then re-installed the door switch. After that, I put the front door panel back on. Then tightened down the door switch. Finally, I installed the top front panel and then the top of the washer.
Parts Used:
Bellow To Front Panel Clamp Bellow To Tub Clamp
  • Matthew from MENTOR, OH
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
2 of 2 people found this instruction helpful.
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Dryer would squeal when the drum was turning
I followed the very informative video and wrote down step-by-step notes for myself. The repair went very smoothly. The only thing I didn't realize, was that the dryer has 4 rollers, not just 2 shown in the video. All are easy to access once you disassemble. I had to do it twice since I had to order 2 more rollers in order to replace them all. Also, the triangle plastic washers come with the roller, so you won't need to order them separately like I did. I also changed the idler pulley roller while I was in there since that has bearings too. Just as easy. I'm very happy with my quiet dryer! One last note: The new rollers are a bit louder than normal at first, but they quiet down very quickly as you use the dryer. It must be because they are brand new.
Parts Used:
Dryer Drum Support Roller
  • Clinton from MINOOKA, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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All Instructions for the MLE20PDCGW0
61 - 75 of 219