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MEDE300VF2 Maytag Dryer - Instructions

All Instructions for the MEDE300VF2
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Loose electrical wiring in dryer shorted causing connection to melt.
Replaced power cord, terminal block, and all melted wiring. Checked the thermal fuse for zero resistance.
Parts Used:
Dryer Terminal Block Dryer Power Cord, 4-ft
  • William from NASHVILLE, TN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Socket set
5 of 5 people found this instruction helpful.
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Screen on the hot air vent disintegrated
It is odd that this part needed replacement but I am in an area near the Atlantic ocean in a vacation house which is vacant most of the year. The exhaust vent probably brings excessive moisture down to the dryer in the basement. The screen you can see at the inside back of the tumbler (where the heated air enters) rotten out, pieces fell inside and there was danger of something falling in and catching fire. I found no useful source for information (including YouTube) as this part is most easily replaced from the rear of the dryer and the available info was about repairing the heating element, the circuit board, or the exhaust venting pieces which is done from the front.

The bottom line is that the back removes easily. You should:
1. unplug and remove the exhaust shoot
2. remove the top per YouTube or other source
3. take off the back panel over the electrical connections and unscrew the ground; tuck it inside. Don't undo any electrical connections except the ground
4. take off the screws holding the back on (8-9, one is hidden above the exhaust vent) and pull it out of the way; you then have compete access to the "DUCT-AIR" part
4. undo the clip that holds the vent tube (from the heating element) to the part
5. remove the screws that hold the part to the inside back (3?) and push it out of the way
6. remove the clips and remove the old part
7. reassemble in reverse order

I'm over 70 so I took lots of time and breaks but was still done in under two hours. The 2 clips holding the heater element tube to the part were badly rusted and should have been replaced but I made do with the old ones.
Parts Used:
DUCT-AIR
  • Thomas from Edgartown, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Drum support roller making very loud noise
had to take front off of Dryer then was able to replace drum roller
Parts Used:
Roller Support Tri-Ring Drum Support Shaft - Rear Shaft with Left Hand Threads WPW10359272 Dryer Drum Support Roller
  • William from TROY, AL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Dryer would not heat
On this model do not try to remove the back. You must remove the bottom front panel and the lint screen unit. You can then loosen the heat coil assembly and rotate it to get to the high-limit thermostat and the thermal unit. I replaced both because I bought the kit. It actually took me longer to clean out lint than it did to replace the parts. A simple remove of the parts with a 1/4 inch nut driver did the trick. Now my dryer works fine.
Parts Used:
High Limit Thermostat and Thermal Cut-Off Kit
  • GARY from PARSONS, KS
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Noisy
Disconnect power supply, remove power cord from dryer, remove dryer vent tube from dryer, remove 2 Philips screws from power connection on dryer, remove nuts from back of dryer, remove back of dryer. Locate idler pulley at bottom of unit at the rear of the motor, pull pulley back to loosen belt and remove from pulley, remove pulley retainer clip, remove pulley and rear washer from shaft and inspect shaft for wear or rust. replace washer and pulley (no specific direction to replace them, washer first then pulley). Reverse above procedure to reassemble. This is for a front load dryer, a top load dryer is different.
Parts Used:
Idler Pulley
  • Robert from HAGERSTOWN, MD
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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Lint filter seal worn out
The part wasn’t for my machine. Unfortunaly I was not able to repair it. I was sent stripe of foam with an adhesive strip on the back. I needed a felt strip.
Parts Used:
Dryer Seal Outlet Housing
  • Dennis from PALM BCH GDNS, FL
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
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part of door hinge was worn and allowed door to sag
removed door by undoing screws holding it on dryer.
Removed all screws on door EXCEPT the ones with star heads.
Separated two parts of door and undid screws holding hinge in place.
Removed hinge and replaced with new hinge.
Put two faces of door back together and installed door back on dryer.

To be honest and explain, I had previously taken apart the door and removed the star screws which allowed the other pieces of the door holding the window to fall apart.
After some difficulty, I was able to put the seal back on and re-install the metal window holders which is why I said it only took 15 minutes after the part arrived and why I accented NOT removing the star screws.
There were a couple of other screws which probably didn't need removing but they didn't cause any problem with the installation.
After putting the door back on, I had to manually twist the door a small amount because it didn't want to keep the button depressed which kept the motor running which turns the basket and heats the clothes.
The door had been causing some trouble for a couple years and we had obviously closed the door with a little extra force when it ''caught'' on the door frame causing it to bend a small amount.
It only took one adjustment and worked fine after that.
Parts Used:
Dryer Door Hinge
  • Barry from ALLEN, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
5 of 5 people found this instruction helpful.
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Old lint filter was broken
Just replaced the old lint filter.
Parts Used:
Lint Filter
  • Earl from Santa Ana, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Dryer made squeaking noise, then more of a rumbling noise.
Checked this site for most likely needed parts and ordered. Located full repair manual inside unit after removing lid. Followed instructions in manual to take apart and remove the drum; took pictures at each removal step and used pill organizer to keep screws in correct order and quantity. The metal cylinder in the center of the idler pulley had ground away so the idler pulley with bracket was replaced. (There was a lot of metal dust that had to be cleaned.) One of the rollers did not turn smoothly so that was also replaced. After putting drum back in, reversed the steps to reassemble and referred to photos to make sure did in correct order and did not forget anything.
Parts Used:
Drum Support Shaft - Rear Shaft with Left Hand Threads WPW10359272 Dryer Drum Support Roller Idler Pulley with Bracket
  • JAMES from NORTH OLMSTED, OH
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Socket set, Wrench set
5 of 6 people found this instruction helpful.
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Idler pulley seized
The pulley is accessible from the back of the dryer. Disconnect the gas line. Remove all the screws. Also remove the small plate that secures the line cord. Lift the back up and out. I was able to avoid disconnecting the water line. Take a picture of the pulley so that you will have a record of the belt routing. Release the spring and remove and replace the pulley and bracket. Vacuum out the lint. Plug in the dryer to make sure that it works properly before reassembly.
Parts Used:
Idler Pulley with Bracket
  • John from CREST HILL, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
4 of 4 people found this instruction helpful.
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Dryer drum turned hard because rollers were worn
Remove top, front and drum. Top is removed by sliding a putty knife under the front corners and pushing the tabs back. Front is held with screws. Disconnect two electrical connectors. Rollers are easily accessible and changed.
Parts Used:
Dryer Drum Support Roller
  • Paul from STONE CREEK, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
4 of 4 people found this instruction helpful.
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Sqeeking noise fron old worn belt and rollers
Watched instructions, Ordered the kit and repair was fairly easy until the time to line up the cover over the fan wheel. That was difficult part. Would be best to have two people at this point to hold it and align the screw holes. Otherwise its was a fairly easy operation.
Parts Used:
Dryer Repair Kit
  • Randy from HUNTSVILLE, AL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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Dryer was squealing
Disconnected Power cord, removed vent pipe, removed back panel, had to slide top cover off to remove additional screw holding back on. Went down to where the Idler Pulley was, removed old piece by depressing on the spring loaded actuator and slid it off the belt and all. Replaced same as removal.
Parts Used:
Idler Pulley
  • Kevin from VALDOSTA, GA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
4 of 4 people found this instruction helpful.
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My dryer was squeaking with an occasional thump
Watched videos on line on how to repair. Replaced all four Drum Rollers, Belt and Idler Pulley, cleaned out inside of unit.
Parts Used:
Dryer Repair Kit
  • Michael from BOILING SPGS, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Wrench set
4 of 4 people found this instruction helpful.
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Broken Drum Belt
Just like the video, just followed the video
Thanks,
Parts Used:
Dryer Drum Seal with Adhesive
  • Garry from Garland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
4 of 4 people found this instruction helpful.
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All Instructions for the MEDE300VF2
76 - 90 of 341