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GLGH1642FS5 Frigidaire Washer Dryer Combo - Instructions

All Instructions for the GLGH1642FS5
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H2O leaking on final spin
drum vane had a hole in it replaced it using phillips screwdriver removed one screw ,pulled drum vane towards the door then pulled up replaced it reversing the procedure. It actually seemed to fix my leak during spin cycle
Parts Used:
Drum Vane
  • judd from jax, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
14 of 16 people found this instruction helpful.
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Washing machine wouldn't drain or spin. It would run through its cycle, but only agitate.
Use a cup to take the water out of the washer. Get at least three large towels -- you're going to have to sop up the water when you disconnect the hoses.

Take the bottom panel off (2 Phillips head screws). Drain pump is on the right side.

Remove the two screws holding the pump to the metal bottom plate. Use a small socket wrench and/or a screwdriver. I had to use a screwdriver on the right screw and a socket wrench on the left screw! Place as many towels in the cavity as you can to catch the water that's going to come out when you detach the hoses.

There is an inlet hose and an outlet hose, attached with bright green clamps. Remove those with pliers. Clean up the water that drains out. The hose in the back (inlet) has a "coin catcher" area. Clean this out.

Attach the hoses to the new pump. Screw it down. Replace the bottom panel.
Parts Used:
Drain Pump - 60Hz 120V
  • Jen from Lebanon, OH
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
15 of 19 people found this instruction helpful.
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Drained but would not spin
The hardest part was figuring out how to get the lid off. You simply remove two screws from the back of the lid and jerk and slide the lid towards the back of the machine. Take out the screws that hold the front panel on, tilt the front out and access the lock/switch assembly and replace.
Parts Used:
Front Load Washer Door Lock and Switch Assembly
  • Gregory from Louisville, KY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
15 of 20 people found this instruction helpful.
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Cracked vane in washer
Removed (1) philips screw in toward back of vane (closest to rear of drum), pulled the vane forward to remove it, slid the new one in place, replaced the screw, and was done in less than two minutes. Piece of cake.
Parts Used:
Drum Vane
  • William from Juliette, GA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
15 of 21 people found this instruction helpful.
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Dryer not working
After reading about similar problems people have had with this make of dryer, I focused attention on the thermal limiter. I determined that it was the culprit by "jumping" it with a 6" piece of wire. Then I simply went on the site, ordered the part. It arrived a few days later and I pulled out the old one, screwed in the new one, and the dryer is good as new.
Parts Used:
Thermal Limiter - Limit 220
  • Susan from Point Pleasent Beach, NJ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
14 of 18 people found this instruction helpful.
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Noise During Spin Cycle
Using a cordless drill and driver bit I removed the back cover, bottom front cover and top. I then removed the rubber bellowed hose connecting the soap dispenser to the rubber boot in front. This one was tricky to reinstall because the fastener for the hose is twisted steel wire that needs to be undone when reinstalling. It slid off easily enough but would not slide back on easily. There is a second small bellowed hose that connects the dispenser to the outer drum casing. This needs to be removed as well. It comes off easily and went back on easily. I used a one sided razor to cut the glue dots connecting the front boot to the washer door frame. After that I removed the belt from the motor and drum pulley by hand and then removed the motor mounting bolts using a ratchet and socket. This went smoothly. I now propped up the drum using 4x4 cutoff blocks to take the weight off the springs and shocks. I then removed to the lower upper plastic pins that hold the shock onto the plastic spin drum casing. I used a wooded block and a hammer to tap the pins out. Be sure to push in the lock on the tapered end of pin shaft. The second pin was a little more difficult to remove and required quite a bit of tapping to push it all the way through. I tried adjusting the weight on the shocks several times to make it easier to come out. The pin was slightly damaged by the time I got it out from hitting it. It went back in OK so I don't think the damage will cause any problems. Next I got someone to help lift the drum to release the weight on the springs and removed then from the top end. You need to remove the spring clamps that hold the spring down at the top end. I used a wrench to remove the bolt that holds the pullet on the drum shaft. The pulley was easy to pry off shaft by placing two flat screw drivers between the shaft and the bearing casing and twisting the screw drivers. Once the pulley was removed I turned the spin drum casing upside down and supported the outer casing with two stacks of 4x4 cutoff blocks. This would allow the stainless steel drum to be supported above the floor and drop freely as the shaft worked it way out of the bearing casing. Getting the drum shaft out of the outer housing bearing was the most difficult part of this whole process. The shaft was rusty and therefore did not easily slide through the two bearing casings. Before hitting the drum shaft to remove it from the bearing casing I put the washer and bolt back on the shaft to protect the shaft from hammer/mallet damage. I tried a mallet but it only moved the shaft part way and then it wouldn't slide further. I then used a 1/2" steel pipe cutoff as a punch seated around the pulley bolt to alloy me to use a hammer to beat the shaft out of the bearing casing. It required a tremendous amount of force to move the shaft. Once the shaft was removed from the old drum casing I spent some time cleaning the back of the stainless steel drum including using emery cloth to remove the rust from the shaft and polish it the best I could. Be sure not to damage the brass bushing that the rubber bearing seal rides on to prevent water leakage. Once the drum and shaft were cleaned up the reassembly process when smoothly I simply reassembled the washer in the reverse order or the disassembly. The shaft went into the new bearings snugly which I was pleased to see since the snug fit meant that the water would be sealed in and the drum would spin true. The hardest part was reattaching the large bellowed hose onto the soap dispenser because it require undoing the twisted steel wire clamp and getting it back together in a very tight space. I use a combination of a flat screw driving and a needle nose pliers to wrestle it back together. The finished job resulted in a very quiet smoothly operating washer which we expect will give us another 5 years of service.
Parts Used:
Rear Outer Tub Assembly
  • Bernie from Point Roberts, WA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
13 of 15 people found this instruction helpful.
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No heat/intermittent heat. Ignitor glowed but no gas flame.
White Westinghouse WDG547PB Dryer. Removed access panel (lower left front of dryer) by removing phillips head screw below access panel. Removed two phillips head screws holding bracket that holds coil in place. Removed coil, disconnected electrical connector. Connected electrical connector to new coil and set in place. Repeat for second coil. Reinstall bracket and access panel. Job complete. Dryer back in service with no problems.
Parts Used:
M Series Ignition Coil Kit
  • Jeffrey from Richmond, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
12 of 13 people found this instruction helpful.
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Water wouldn't drain from washing machine and clicking sound when trying to run
Used a shop vac to suck all the water through the drain hose. Removed the bottom front panel held by two screws on bottom and two plastic pins at the top. Removed electric connector on front of pump. Removed two screws holding pump down. Used pliers to move spring clips back so hoses could be removed. Put hoses on new pump and squeezed clamps with pliers to pull them back over the hose connection. The connection on the left was a little bit of a pain due to space limitations. Screwed the new pump down and reconnected the electric plug. Put the bottom cover back on and screwed it into place.
Parts Used:
Drain Pump - 60Hz 120V
  • Bruce from Alfred Station, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
12 of 13 people found this instruction helpful.
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door assembely had a snapped piece of plastic in unit.
I released the door gasket and unscrewed the unit .Labeled the connections. then reconnected reattached, then put gasket back on. Worked like a charm!
Parts Used:
Front Load Washer Door Lock and Switch Assembly
  • DANIEL from STRATFORD, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
12 of 14 people found this instruction helpful.
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Stainless tub in front loader broke 2 out of 3 spider arms
Removed entire tub assembly, replaced bearings and seal in rear outer tub assembly, had spider arms welded by aluminum welder. alot of work ,saved 150.00 on parts by replacing bearings, savings untold hundreds by doing it myself instead of replare man.. BIG JOB. But just plug away and it goes rather smoothly.
Parts Used:
O-Ring/Gasket
  • Ed from International Falls, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
13 of 18 people found this instruction helpful.
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Tub to pump hose leaking
From the front of the washer, I removed two sheet metal screws at the bottom of the access panel. The panel pulled off with a just a little effort due to the nylon inserts installed on either side of the panel that keep it in place. The tub-to-pump hose is located on the right hand side and easy to access. The hose includes a screw clamp and two tension retainer (?) clamps that need to be removed.Make sure to save them for the new hose! I used a phillips head screwdriver for the screw clamp and a pair of channel locks to remove the tension retainer clamps. The tension retainer clamps were easy to remove but tricky to put back on. There must be another tool used for them that I'm not familiar with. With just a little patience though, it's an easy enough repair for anyone to do.
Parts Used:
Tub-To-Pump Hose
  • Barbara from Los Angeles, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
11 of 13 people found this instruction helpful.
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Falling apart!
It started out with the tub not draining. No problem, has happened before. Remove bottom panel, take boot off of extractor motor, clear out book & check impeller for obstructions. Noticed belot was off. Got new belt. Belt would not stay on, bearings shot. Bearings are pressed into rear outer tub shell. Must remove pulley to get tubs apart. Good luck! Pulley was corroded onto shaft of inner tub. Used various tools, finally ended up grabbing hammer and beating it. Screwed up threads, broke pulley, but got it apart. Re-tapped threads, ordered new pulley. Finally got everything together. Worked intermittantly. Thought it was motor going out. Ordered new motor. It was door switch. Done spending money, bypassed door sensor. Whew! We have clean clothes! Ended up costing about half the price of a new unit, but it basically IS a new unit! Plus I have a spare motor for when that finally goes out!
Parts Used:
Rear Outer Tub Assembly
  • Michael from El Cajon, CA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
12 of 16 people found this instruction helpful.
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Thumping vibration on spin cycle
Remove the front lower panel. Remove the 4 plastic pins mounting the shocks using 1/2 inch short socket to hold the detent down as per included instructions. All plastic pins were stuck in place so used needle nose pliers to pull or push out. Lube the pins with grease before reinstall to help them go through the new shocks. Use the included lock nuts to lock the four legs in place as low as possible. Start the washer and level each leg while running so you can tell if the vibration is going away. Tedious method but worked.
Parts Used:
Shock Absorber Kit
  • Kerry from Pasadena, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
11 of 13 people found this instruction helpful.
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The drier was "screeching"
First of all, the folks at Part Select have been terrific. I balled up my address and they were great in correcting my error and getting the parts promptly to me. They provide directions with the parts. And You Tube, is a wealth of information too. The process is to remove the drum and replace the nylon busihing that supports the drum at the back of the machine. Getting it out was no sweat. Getting the drum back in was a bit more challenging single handed. If I was going to make any suggestion it would be this is a good project for two sets of hands with the second set needed for about ten minutes. The You Tube video I watched said putting the front cover with the drum attached to the back of the unit would be the challenge and they were right. Otherwise, super easy and the results are it's back to "new" condition. Thanks again to Part Select!
Parts Used:
Rear Drum Bearing Kit Rear Drum Bearing Kit Drum Support Bearing Rear Drum Bearing Kit
  • Michel from CHICAGO, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers
9 of 9 people found this instruction helpful.
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Felt around drum holder worn and torn.
1. Removed face of dryer (drum 'holder')
2. Disconnected door switch wires
3. Tore off existing felt

NOTE: The length of the felt that I recieved from PartSelect was incorrect (too short). Since the existing felt was worn and torn at the top, I replaced only a length that matched the length of the new felt.

4. Used a razor blade-type gasket remover/scraper to remove the exisitng glue
5. Applied new glue (which comes with the felt) onto the felt and let it set up

NOTE: In hindsite, I would apply the glue to the drum holder instead, as the glue otherwise soaks into the felt. If applied to the drum holder instead, the glue will spread out and provide more surface area for adherence.

6. Installed the new felt, starting at one end and working my way around to the other end, being careful not to stretch it
7. Trimmed the remainder of the existing felt (see first NOTE)
8. Scraped the drum holder below the pulled away ends of the exisitng felt
9. Applied glue to the existing felt, including the trrimmed ends so that the ends do not pull away from the ends of the new felt
10. Re-attached the existing felt
11. Let the glue set-up overnight
12. Reinstalled the face of the dryer, turning the drum so that the felt will not get pushed away
13. Reconnected the door switch wires
14. Turned dryer on, with lid still raised, to check for any drifting of the felt
15. Once assured that the felt would stay in place, put the dryer in service

NOTE: I replaced the felt becasue of the gap that opened due to compression of the felt. The gap, as well as a torn piece of the felt that entered the interior of the drum, was catching clothes and tearing them as they were rotated between the drum and the drum holder. The new felt eliminated this problem.
Parts Used:
Lower Front Felt Seal with Adhesive
  • Robert from York, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
10 of 12 people found this instruction helpful.
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All Instructions for the GLGH1642FS5
76 - 90 of 632