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AGQ6000ES2 Frigidaire Dryer - Instructions

All Instructions for the AGQ6000ES2
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Drum would not spin
After unplugging the dryer, disconnecting it from the vent, and moving into an open work area, I popped the top open with the blade of a screwdriver, disconnected the two wires that connect to the door switch, then lifted the front panel (with the door) up and away from the drum. Next, I lifted the drum out of the worn rear bearing assembly and lowered it into the dryer in order to release tension on the belt. I then removed the entire drum by carrying it forward and out of the way. I then removed the old bearing assembly, which was loose and covered with metal dust. After cleaning the area with a dry cloth to remove the old grease and metal dust, and vacuuming all the lint off *everything*, I installed the new bearing assembly with a 5/16" nut driver, being careful to position the provided ball-bearing between the plastic bearing assembly and the outer clip. The little ball-bearing is very important, as it is the drum's only path to ground, and prevents the build up of static electricity as the drums spins. I then filled the new bearing assembly with the provided grease. Everything is easy up to this point, but the difficult part for me was removing the old hub from the drum and re-attaching the new one. It is held on by three screws and they become seated very tightly. After loosening them and removing the old hub from the drum, attaching the new one prvoed difficult as well, as the screw-holes in the new hub are not threaded to fit the screws. The screws muct be forced to cut a thread as you install them, which requires a great deal of force. After installing the new hub and putting the new belt (pruchased separately) around the drum, the next step is to reinstall the drum by lifting it in through the front of the dryer and positioning the new hub over the new bearing assembly and pressing it down into place. It will gently "snap" into place as it seats. Then, on the back side of the dryer, I removed the vent panel by removing the two screws that hold it in place and positioned the new drive belt (loosely dangling around the drum) over the motor's drive wheel and behind the sring-tensioned idle arm. Then it is a simply matter to reinstall the front panel by genly lifting the drum and sliding the door opening inside it, then reseating all the little clips that hold the front panel in place. I then pressed the top back into place, reconnected the vent hose, plugged it back in and checked for operation. My fifteen year-old dryer now works like new!
Parts Used:
Drum Belt Rear Drum Bearing Kit
  • garland from Morganton, NC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Gas flame turns off after a while, dryer keeps turning but no heat is generated.
Before this fix which worked beautifully, I tried replacing the flame sensor which did not work. To read that story, search under part number PS459818 (Flame Sensor). Our model is a Westinghouse, so access to the unit is a bit different than the other stories. It's a stacked front-loader sitting on top of a washing machine.

1. Open the little front door (lower left side) by unscrewing the little screw right below it. The door will pivot and slide out vertically.
2. Disconnect the electrical main lead coming from the back of the unit (just in case).
3. Close the gas switch lever on main gas pipe coming from the back on left side (just in case).
2. Remove 2 phillips screws on top of the metal bracket holding the two coils. The screws have to be removed completely along with the bracket. It's easy, they are right in front and there is room for the screwdriver. Use a thin long one instead of one with multiple bits to better align with the screws, which are very close to the coils.
3. The two coils slide right out and are very different so it's easy to keep them straight. Remove electrical connectors before or after removing the coils (I marked the plastic on top with a sharpie to keep them in the right orientation).
4. Drop in the two new coils and reconnect them to the electrical leads.
5. Reconnect main electrical lead from back (match wire colors)
6. Reopen gas lever on gas pipe.
7. Drop in front cover at an angle, tilt vertically and put screw back underneath. Use magnetized screwdriver or a piece of scotch tape to hold the screw or it might fall off the screwdriver.
8. Voila'. It worked.

This website is great. Our dryer is a Westinghouse bought in 1991 (almost 20 years old!) and with this fix it's just like new. In 1994 we used parts bought here to fix our washing machine (Westinghouse LT350RXW1). That machine is now 15 years old and still going!
Parts Used:
M Series Ignition Coil Kit
  • Giuseppe from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Control panel was fried and started only displaying error codes; dryer didn't run
We took off the top of the dryer and then the front panel. The hard part was that the new control panel was a bare circuit board and did not come encased in plastic housing. So we had to remove the "old" plastic housing from the old panel and assemble it with the new circuit board. If you're used to this kind of repair and know what you're doing, it probably wouldn't be very difficult. But since we were complete novices, it took some finessing and head-scratching to make sure we were doing the right thing. And even then, we didn't know it was "the right thing" until we plugged the dryer back in. I feel like we got pretty lucky that it worked. But we are happy that we took the chance.
Parts Used:
Control Board
  • Michelle from S PASADENA, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers
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No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
Parts Used:
M Series Ignition Coil Kit
  • Steven from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
2 of 3 people found this instruction helpful.
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loud squeeling noise
After changing the drum support bearing, and the front felt ring, the noise continued. It turned out to be the tensioner pully. The harmonic vibration travels throughout the dryer box like an instrument so you can't tell where the sound is comming from. Before you do anything, spray a little wd40 between the bushing and the shaft on the belt tenioner pully. If the squeel goes away, you have found your smoking gun.
Parts Used:
Drum Support Bearing
  • Lewis from Thornton, CO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Dryer making horrible squeaking sound when running
I am a "do-it-yourselfer" despite my husbands opposition. I followed instructions from one of the posts on the site and took apart the dryer. I found the location of the rear bearing and took it out and replaced it with the new one. Easy as that. Made sure the parts looked the same. Made sure I saw how everything went together. I used a magnet to hold the ball bearing in place on the rear mount and taped the metal bracket on the outside of the dryer. Screwed it right in. Reassembled in reverse and works like a charm. To all the women out there who don't think they can do this. It's easy. Give it a try.
Parts Used:
Rear Drum Bearing Kit
  • SHARON from SUMMERVILLE, SC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench set
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E66 Error code, Door Open. Dryer shuts off on high temperature
Unplugged dryer. Removed top panel (2 screws top back of dryer). Removed control panel ( Unplugged from control board and 2 screws) Removed front panel with door ( Unplugged light from control board, door switch at connector, and 4 screws) Removed Control Thermister from dryer exhaust blower housing located bottom front of dryer ( Unplugged 2 wires and removed 2 screws ) Installed new Control Thermister and replaced all screws and panels in reverse order. Note: Noticed connector for door switch seemed a little loose when connected correctly. Used electrical tape to reinforce connection. Plugged dryer back in and checked operation. Dryer has been used approximately 10 times since repair with no issues.
Parts Used:
Control Thermistor
  • Michael from Baltimore, MD
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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door catch wasn't working and screws in door were loose.
popped the catch in existing hole and replaced the screws
Parts Used:
Door Catch Screw
  • NICOLE from WEST JORDAN, UT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Latch on dryer no longer worked
So easy! I ordered the part on the website. Received it 24 hours later. And popped it in place. Good as new.
Parts Used:
Door Catch
  • chris from dallas, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Our door catch got lost inside the dryer after the door was slammed to hard
I took the new door catch out of the packaging and just snapped it in place it was easy peasy and took less time than opening the package
Parts Used:
Door Catch
  • Joyce from PORTAL, GA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
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bearing bad and shaft broken
replaced bearing and shaft new belt and everything works just fine
Parts Used:
Drum Support Bearing Rear Drum Bearing Kit Dryer Drum Bearing Bracket
  • Randall from New Roads, LA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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Had a squelch/squeak coming from the rear of the unit
I looked up a YouTube video on my specific model. Found one that said “basic disassembly”. I watched that and had it apart and back together in no time. Very easy to take apart and put new parts back in it. Re-assembled and since the repair no squeaking.
Parts Used:
Drum Belt Rear Drum Bearing Kit Drum Support Bearing
  • Stephen from HICKSVILLE, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Broken belt
Watched video sent to me after I purchased belt on line. Super helpful!
Parts Used:
Drum Belt
  • Sharon from UXBRIDGE, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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load squeal
replaced rear drum bearing kit. Watched video made it real easy. The only problem was getting the belt back on the pulleys.
Parts Used:
Rear Drum Bearing Kit
  • Mark from HGHLNDS RANCH, CO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Loud squealing
As all others have said, without being redundant, I'd view post #1 or #2 for a good detailed set of instructions.

The primary issue I had was with the stainless steel ball bearing that was shipped with the kit. I couldn't figure out what it was used for, because when I removed the bearing carrier the ball fell out before I could see where the original one was located. The stainless ball bearing is a grounding ball, not a bearing. It goes on the exterior of the plastic bearing carrier/receiver.

Once I figured that part out, it was a piece of cake.

Took a little longer than other people's repairs, but I also put a new belt on and re-worked the exhaust duct for solid ducting versus flexible duct. fine-tuning the rigid duct work was a piece of cake with the tumbler out, since i could crawl right inside the chassis and make sure everything would line up (level legs, adjust elbows, etc)
Parts Used:
Rear Drum Bearing Kit
  • John from Avis, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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All Instructions for the AGQ6000ES2
91 - 105 of 329