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LSE7806ABQ Maytag Washer Dryer Combo - Instructions

All Instructions for the LSE7806ABQ
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belt was slipping
The job went fast an well
Parts Used:
Belt Kit Belt Kit
  • ROBERT from MORGAN CITY, LA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
38 of 50 people found this instruction helpful.
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Washer motor start windings burned up
The motor was easy to replace: unplug the wiring harness, slip off the belts, release the tension springs from the motor carriage with needle-nose pliers, and then unbolt the motor carriage with socket set and remove from the washer. Remove the pulley from the old motor with allen wrench and transfer the carriage to the new motor. Reverse operation for everything and you are back in business. The hardest part was the far back screw holding the carriage, a wobble extension helped.
Parts Used:
Drive Motor - One Speed - 120V
  • Eric from Seabeck, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
36 of 47 people found this instruction helpful.
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The water didn't pump out during the spin cycle
I took out the two screws in the bottom front panel of the washer, and rotated the front panel from the bottom away from the machine until the top or the panel was released from the machine frame. I then tilted the washer back to get access to the bottom of the machine. The pump pulley had split in half, and the bottom half fell off the drive motor shaft. The only problem I had was breaking free the set screw that holds the pulley to the drive motor shaft. I used a long arm Allen wrench and an adjustable "Cresent" wrench to apply enough force to break the set screw loose. Iclamped the upper transmission belts tightly to keep the motor shaft from turning while I loosened the set screw.
Parts Used:
Motor Pulley
  • Robert from Menomonee Falls, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Wrench (Adjustable)
30 of 38 people found this instruction helpful.
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Broken contact on high limit thermostat - dryer no start
First I unplugged the dryer! Then unscrewed the two screws at the bottom of the front door. To remove the front door, swing the bottom up about 30 degrees until the two triangular hooks at the top of the door release. Then release the two wires going to the door switch from their harness so as to gain more slack to move the door out of the way. The switch was secured by 2 hex head sheet metal screws1/4inch in diameter. I used a small right angle socket wrench to get these loose. I only had to remove the front screw completely to be able to take the switch out for exchange purposes. Once this was done, reverse the process and plug it in! (BTW, the electrical schematic for this dryer is up under the top console)
Parts Used:
High Limit Thermostat (Limit: 200-30)
  • Nova from Hudson, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set
30 of 38 people found this instruction helpful.
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Very loud intermittent squeeling when running
Remove top two front cover screws. Disconnect wiring. Set aside front cover - door assembly.

Remove two screws at top of the vertical riser cover to expose entire dryer interior. Remove filter. Remove screws to blower cover plate. Remove 4 screws that fasten front drum guide assembly. Remove drum. remove and replace 2 drum support rollers . Replace one rusted drum roller shaft. Replace both drum rollers and non-metalic washers.

Drill out 4 rivets holding two front drum glides. Replace and rerivet new drum glides.

Pry back slighty the many retention points around the front drum assembly which hold the front drum felt seal. Refit the new front drum felt, pressing the retaining clips back in place with a screwdriver.

Replace tumbler motor belt.

Install Drum. Install front drum retention assembly. Install new blower seal with reassembly of blower cover.

Total time - about 1 hour
Parts Used:
Tumbler and Motor Belt Roller Shaft Dryer Blower Housing Seal Roller Shaft Hex Nut Front or Rear Drum Felt Seal Drum Roller Shaft Washer Front Glide Kit Drum Support Roller Kit
  • Tom from Blue Bell, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
26 of 29 people found this instruction helpful.
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Heard squealing sound when washer went into the "spin" mode. Tub did not spin
Replaced the 2 belts according to instructions received with the belts. Very easy repair
Parts Used:
Belt Kit Belt Kit
  • Edward from Stroudsburg, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
28 of 36 people found this instruction helpful.
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Strange noises - drum not always emptying
Found a very stretched, loose pump belt. Was able to pull it off pump pulley and motor pulley easily. Pushed motor assembly toward transmission pulley and removed wider drive belt. Wiped all pulleys clean. There's a double on the motor- one for drive belt, one for pump belt. Removed two hoses from pump using nutdriver. Removed pump. New pump installed. Installed two hoses on new pump. Installed drive new drive belt. Installed pump belt last. Slid pump to near farthest spot in slots. Tested for correct tension by pinching pump belt. Should be able to pinch center so two pump belt sides come within 1/4" of each other just as the spring tensioned motor mount starts to move. Pused washer back into place after external hoses connected. All new hose washers and filters on both hot and cold. Ran, checked for leaks - none! Absolutely perfect. Put front panel back on. No weird noises and drum empties perfectly every time. My wife is so pleased she's doing more loads.
Parts Used:
Drain Pump Belt Kit Belt Kit
  • Kenneth from Sunnyvale, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
26 of 31 people found this instruction helpful.
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Dryer stopped working
From previous experience I suspected the thermal fuse. Turned off the power and removed the front of the dryer by removing the two philips head screws in the door hinge and the two screws on the opposite side of the opening. The front came off easily since all that holds it in place besides the 4 screws are two spring clips. The thermal fuse is located on the side of the chamber enclosing the heating element. I removed the wires connected to the thermal fuse and temporarily joined them together with a spade type connector in order to determine if the thermal fuse was the problem. Turned the power back on and tried the dryer......it ran normally. Turned the power back off and removed the thermal fuse by taking out th two screws with a 1/4" nutdriver.
Ordered a replacement thermal fuse, installed it (with power turned off) and put everything back together. Dryer functioned normally after the thermal fuse had been replaced.
The thermal fuse can be removed and reinstalled using a 1/4" nutdriver. The wires are connected with push on spade type terminals.
Note: The swing damper on the dryer vent (the hooded cover where it exhausts to the outdoors) was jammed in the closed position with an accumulation of lint, which caused the dryer to overheat and blow the thermal fuse. If you experience a blown thermal fuse, always look for the cause or you'll blow the replacement within minutes of running the fryer again.
Parts Used:
Thermal Fuse
  • Mary Ann from East China Township, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
25 of 30 people found this instruction helpful.
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Water inflow did not stop = flooded utility room
Cleaned up a wet utility room floor!

Unplugged power cord to the machine and turned off hot and cold water at the stop valves.
Removed the top machine screw that holds the metal panel with the valve attached (on the rear of the machine where hoses attach), removed it from the machine with valve and hoses attached.
Disconnected both water hoses at the old valve, together with the 1/2" hose to the machine. Mark hot and cold positions.
Moved the electrical contacts one-by-one to the new valve.
Changed the old valve for the new valve (one screw attaches to plate).
Connected the inlet hoses and 1/2" hose to the new valve, making sure hot/cold on correct positions.
Replaced plate in the machine and secured with the machine screw.

*** NO MORE WADING SINCE REPAIR *****
Parts Used:
Water Inlet Valve
  • Kevin from Chico, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
23 of 25 people found this instruction helpful.
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washer wouldn't let the water spin out!
I was told that it might be a clog in the tube.. we check the tubes that wasn't it Then I Google it and was told it might be the drain pump. I was just glad that Part Select had what I need because my machine is over 20 years old. We change the pump and now I hope I get at least another 20 years out of my machine. I will always use part select to get my parts. Thanks
Parts Used:
Drain Pump
  • SHARON from DETROIT, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set
22 of 23 people found this instruction helpful.
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Rattling sound.
Turned off circuit breaker. Removed two screws at base of front panel with stubby Phillips-head screwdriver. Swung panel up about 30-degrees, and removed panel, disconnecting red and yellow wire to door switch. Removed four sheet metal screws and took off large drum support bracket. Checked drum support rollers and shafts. They were fine. Reset circuit breaker and turned on dryer. Rattling noise still present.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Laurence from Leesburg, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
21 of 24 people found this instruction helpful.
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Dryer was making awful noise during use
Removed the screws and took the door off then took the front panel off and popped up the top. Then pulled the drum out. Took snap ring pliers and removed rollers and replaced with new rollers then vacuumed all lint from machine and reversed operation to put everything back together. Operation was a total success!
Parts Used:
Drum Support Roller Kit
  • Pam from Aberdeen, WA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
20 of 22 people found this instruction helpful.
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Plastic thing (Fill Injector) that puts water in the washer broke
Unfortunately, I couldn't find instructions for removing the top for exactly this model. First step was to remove the front panel by removing the two lower screws, grabbing the bottom of the panel, and lifting up until the clips on top of the panel let go. Next was removing from underneath the two screws towards the front that held the top of the washer on. This gives you easy access to the Fill Injector, but if working alone you'll need something to prop up the front of the top lid while you work on it. There is one screw that hold on the Fill Injector assembly (top and bottom). This screw is removed from the top, via the control panel. To get inside the control panel you need to remove the back of the control panel (very easy), just unscrew the 5 screws on the back of it. Then remove the one screw that holds the Fill Injector assembly in place. From under the front panel, use your pliers to remove the hose clamp and then remove the Fill Injector from the hose. ONE IMPORTANT ITEM, YOU'LL DEFINITELY NEED A REPLACEMENT HOSE CLAMP. The one you remove to take off the old, broken fill injector cannot be put back on. Put the new clamp loosely on the hose, then connect the hose to the new Fill Injector Assembly. Put the Fill Injector Assembly in place and use a piece of duct tape to hold it there. Then reinstall the screw that holds it in place from the top, inside the control panel. Reinstall everything in reverse, give it a test and then have a beer. You've just "given it to the man" and saved yourself $100+ on a repair bill.
Parts Used:
Upper Fill Injector Lower Fill Injector
  • AMY from Mount Kisco, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Socket set
19 of 20 people found this instruction helpful.
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Washer drum not spinning correctly
Drum on the Maytag washer was not spinning is a true rotational pattern. Adjust or replace the centering springs.

How-to-description
I had to hack saw off the centering springs eye bolts since they were rusty and not adjustable. If you have to cut the old eye bolts as I had to, be careful... the spring will jump up an inch or two very quickly and you want to keep your hands clear. It makes a load noise and my wife asked "what happened". Not a big deal, just be aware of the spring returning to a normal state.
Place the new eye bolts in position and tighten the nut with 4 turns. With duck tape I held the eye bolts in place from under the machine. Had my son push the drum towards the replaced spring to shorten the length of the end of the spring to the eye bolt. Stretch the new springs with a long screw driver, one end against the washer body, and the other end near the handle. Pulled down on the scrw driver until the spring can hook onto the eye bolt. Before cutting the old eye bolts I measured the length of the eye bolt from the spring to the frame. Adjust the new eye bolts to the same length after the spring is stretch onto the eye bolt. Overall a simple project, cost $40 for me and the best advice is using the long screw driver to pull down on the springs.
Parts Used:
Centering Spring BOLT Eyebolt Nut
  • Paul from Huntley, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
21 of 27 people found this instruction helpful.
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Washer leaking badly and making loud noise on spin
Determined the tub seal was bad and ordered the seal and tub bearing. Removed the front cover with two phillips screws and unbolted the top to lift back. Removed the agitator with 1/4" setscrew on side and lifted out. Using punch and hammer, broke the inner tub nut loose (clockwise is off). Lifted out the inner tub, unscrewed springs from the bottom and removed; then removed the bearing with a little prying (had to raise the tub slightly and tap the center splined shaft to push out) and lifted out the outer tub. Outer tub had few rust spots about to penetrate, so sanded off rust, primed with etching auto primer and sprayed enamel topcoat to prevent further corrosion. Reassembled in the same order.

When done, there was still a loud noise on the spin cycle, so obtained a spin bearing and brake assembly (need to replace both most always). Tilted the machine on its back and removed the pulley, then put a special wrench on the brake assembly and broke loose (counterclockwise) with a 3 foot extension after placing a 2x4 section in the tub between wall and one of the bases for the spring arms (to keep the tub from turning). When the brake came off it was full of water and corroded from the leaking tub bearing previously replaced. Reassembled in reverse order and replaced two belts on the bottom for good measure. Works perfectly now and is very quiet.

In my estimation, the repair should have included both the tub bearing/seal and the spin bearing/brake assy from the outset. Could have used a chain visegrip wrench instead of special tool to remove the brake assy - whatever is available. The tool costs a lot and will never be used again.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Barry from Brooklyn, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
19 of 22 people found this instruction helpful.
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All Instructions for the LSE7806ABQ
31 - 45 of 1054