LSE7804ACE Maytag Washer Dryer Combo - Instructions
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Smoking Washing Machine.
Well, I figured out a couple of things during this process. #1 The Washer was smoking. It had happened before (a sock got suck between the basket and the tub) so I assumed that happened again. I couldn't see anything in that space this time, so I dissasbemled the washer to see if any clothing was there. Relatively easy once finding the screws to remove the front panel. #2 What I found was a sock in the pump box. I disconnected the hoses and removed it, saw nothing between the basket and tub and ran it to see if problem corrected itself. It still was smoking. That is when I checked the belts, #3 first the pump belt, replaced it, very easy, just pulled the old one off, and wheeled the new one on. It still was smoking, #4 so I replaced the drive belt, very easy and the same as the pump belt. It still was smoking so I lubed the wheels for the belts, and #5 cleaned the residual rubber around the wheel from the old, fried, dry rotted drive belt. No more smoke!!! However #6 remember to leave space between the basket and the top of the tub, as when I put the washer back together the basket didn't spin. I removed the top and ran the spin cycle, it spun fine, reconnected and it didn't spin, the tub top was touching the basket, that's when I relized the top was on too tight. I reattached and left about 1/4 in of space and all is well now.
Parts Used:
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Matthew from Wilmington, DE
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers, Socket set
10 of 12 people
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no water drain
removed old pully, put new one on with hex driver, removed belts, put new belts on and finished.
Parts Used:
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Franz from Lakeland, FL
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
20 of 26 people
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Dryer would not turn start
I troubleshot the repair using the repair help section from Parts Select. It made finding the problem a snap. I then removed the four wires and two screws that held the heating element in place. Removed two screws that held thermal fuse in place and replaced. By accomplishing the repair myself I saved well over a hundred dollars.
Parts Used:
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John from Midway, GA
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
10 of 13 people
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Washer did not drain.
Took front panel off. Ran machine. Pump is see-through. Could not see any "aeration" of the water in the pump and no water was coming out of drain hose. Disconnected electric. Disconnected hose from drum to pump(first emptied ALL water from drom)and drained in bucket. Disconnected drain hose from pump to drain and drained any water. Checked for obstructions in hoses. Removed pump. Checked belt (was fine after 14 years). Ordered new pump. Received the next day! Replaced pump and tighten belt. Connected hoses and test it. All OK. Replace panel and did laundry.
Parts Used:
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Basil from St. Charles, MO
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Socket set
9 of 10 people
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Standing water in washer tub
Thinking the water pump was not doing its job in removing all of the water after the rinse cycle, I replaced the water pump.
1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.
This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.
Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.
This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.
Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
Parts Used:
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James from Baton Rouge, LA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Socket set
9 of 10 people
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tub leaked
followed instructions elsewhere here. Procedure went flawlessly
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.
STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.
STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
Parts Used:
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Fritz from Redway, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Wrench (Adjustable), Wrench set
8 of 8 people
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washer fills with water wont start
checked lid switch ,plunger stuck in the in position 1 amp fuse blown took switch apart it was full of green copper corrosion stopping plunger from moving correctly. replaced switch and fuse and wow washer works
Parts Used:
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JOHN from ERWIN, TN
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
9 of 11 people
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Dryer did not turn off in auto-dry mode
Unplugged the dryer (electric), removed two screws at bottom of front panel and removed front panel. Pulled electrical clips from sensor lugs near center.front of drum exterior. Located sensor inside front of drum interior, removed screw at each end. Removed old sensor, placed new sensor in position, attached with screws. Installed electrical clips on lugs, closed front panel and secured with two screws. Plugged in the dryer and it worked!
Parts Used:
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W. Dale from Newton, KS
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
11 of 17 people
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Washer would fill but not continue the cycle
I looked at the common problems in the owners manual and one item was the lid was not closed or the lid switch was bad. I took off the control panel and there was a schematic inside. This showed 2 lid switches. When trying to see if one switch was closed as it should be, touching the multimeter to the contacts was enough to get the washer going. .
Parts Used:
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Paul from Cedar Falls, IA
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
9 of 11 people
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Motor needed replacing (even though it was only 8 years old!)
In addition to the other helpful suggestions:
The key to replacing the motor is to remove the motor while it is still clipped in to the bracket (after removing the blower assembly, of course.) Don't remove the tumbler and belt thinking it will give you clear access to the rear clip, because it won't.
Removing the bracket is not complicated. There are two screws that are fairly easy to access and keep the bracket in place (refer to parts diagram for location); when the screws are removed, out comes the motor assembly (after disconnecting the wires, of course.) This is the only way to get access to the two clips that hold the motor to the bracket.
As for those pesky clips, I was able to use a flat screwdriver in one hand and vice grips in the other to pry off the clips. After a few tries, working on one end of the clip, I was able to apply quite a lot of downward pressure without braking the end of the clip. If anyone has another suggestion....
Putting the clips back on was much easier. First, remount the motor to the bracket, making sure to rotate the motor to the 2 o'clock position so you can re-attach the ground wire (or else you'll have to unclip the motor again, like I did!) Then re-attach the clip on one side. With the clip aligned properly, bear down with a flat screw driver on the other end of the clip. A swift knock with a hammer on the top of the screwdriver will easily re-attach the clip. Repeat with the second clip.
If you proceed carefully and patiently, this job can be accomplished without specialized tools or expertise.
The key to replacing the motor is to remove the motor while it is still clipped in to the bracket (after removing the blower assembly, of course.) Don't remove the tumbler and belt thinking it will give you clear access to the rear clip, because it won't.
Removing the bracket is not complicated. There are two screws that are fairly easy to access and keep the bracket in place (refer to parts diagram for location); when the screws are removed, out comes the motor assembly (after disconnecting the wires, of course.) This is the only way to get access to the two clips that hold the motor to the bracket.
As for those pesky clips, I was able to use a flat screwdriver in one hand and vice grips in the other to pry off the clips. After a few tries, working on one end of the clip, I was able to apply quite a lot of downward pressure without braking the end of the clip. If anyone has another suggestion....
Putting the clips back on was much easier. First, remount the motor to the bracket, making sure to rotate the motor to the 2 o'clock position so you can re-attach the ground wire (or else you'll have to unclip the motor again, like I did!) Then re-attach the clip on one side. With the clip aligned properly, bear down with a flat screw driver on the other end of the clip. A swift knock with a hammer on the top of the screwdriver will easily re-attach the clip. Repeat with the second clip.
If you proceed carefully and patiently, this job can be accomplished without specialized tools or expertise.
Parts Used:
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ian from new york, NY
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Pliers, Screw drivers, Socket set
9 of 11 people
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Noise in dryer
How to disassemble the dryer has been covered in past repair stories. I will add a make shift repair that will get you up and running until you get your replacement blower wheel. We repair gas dryers for a living and this repair works and some machines are still running for two years. Remove the blower wheel. Cut a piece of plumber strap of similar sized metal to about 3/16" x 1/2". Hold it with vise grips and then heat it with a torch. When it is hot melt it into the hole in the blower wheel. This will give you a flat spot in the shaft hole that will keep the blower from spinning on the motor shaft. Some trial and error fitting is involved. If you do it carefully the blower wheel will fit very nicely and will not vibrate or make noise.
Parts Used:
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Joseph from Hampton bays, NY
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
8 of 8 people
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Floor floded when washer started.
Thirty year old Maytag washer. Remove two screws at bottom of front panel with Philips screw driver. Hinge panel up to disconnect front panel from top of machine. Tilt washer back against wall to gain access to pulley at underside of washer. Then remove Philips head screw from bottom of center shaft. Remove bevel washer with screw. Remove stop block from end of center shaft and wind the pulley off center shaft. Clean center shaft of any debris and lightly coat with grease. Install belt on new pulley and motor, wind new pulley on center shaft. Replace stop block, washer, screw, and front cover.
Parts Used:
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Keith from Big Sur, CA
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
9 of 12 people
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Water leaking into basin when washing machine not in use
Turn off water. Disconnect hoses from washer. Remove drain hose from plumbing drain in wall. Catch water from all three hoses in plastic tub. Remove two 5/15 machinve screws holding inlet valve cover/mount plate. Remove fill hose by compressing hose clamp ends with pliers. Remove electrical connections. Reverse to install. Easy as pie!
Parts Used:
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Tate from Carrollton, TX
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Wrench (Adjustable)
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My dryer - which is about 20 years old - was starting to make some rubbing/scraping sounds from the drum area.
This was pretty much as easy as most other folks had described on this site.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
Parts Used:
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Richard from Loretto, MN
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Difficulty Level:Really Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
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My Blower wheel had broken at the center where it attached to the axle. It made a rattling sound and no air was being blown into the drum to dry the clothes. There was also a loud skidding sound that turned out to be due to a worn felt seal.
I took off the front of the dryer with the screws at the bottom. I removed what wires would easily come off and took a picture to remember where they go. Then I took of the front panel and had to take off the cover for the blower wheel. Some screws were difficult to reach because they were in a very tight space. I used a combination of needle nose pliers and a hex screw bit to loose hared to reach hex screws.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
Parts Used:
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Spencer from COLUMBIA, SC
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers, Socket set
7 of 7 people
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