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CADG265RCL General Electric Dryer - Instructions

All Instructions for the CADG265RCL
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Very loud squeak with drum rotation
Key starting point is to remove top cover by removing two long screws located at the front of the cover
Remove control panel and it's bottom and side supports.
Remove short vent pipe by bending retainer tab.
Support the drum at the top using piece of rope.
Remove main rear cover (leave bottom attached).
Remove electric heating unit and install new bearing carrier from kit.
Reinstall the the heating unit
Remove three screws (inside the drum)to release the inner drum cover and release the bearing carrier.
Install new bearing carrier. Note: the three holes in the bearing carrier are not tapped, I suggest that the screws be installed (threads cut) into the bearing cover before attempting to install the bearing carrier.
Install the new bearing carrier. Note: pilot one of the holes using a small nail etc. then go on to install screws in the other two holes remove the pilot device and install the third screw.
Reassemble in reverse order.
Parts Used:
Rear Drum Bearing Kit
  • William from San Juan, TX
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Wrench set
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Belt broke, tumbler did not turn.
After identifying the issue, the biggest issue was trying to identify how to get the belt around the drum tumbler. After looking through the back hatch, I figured the best way was through the top. I removed the top just enough to work the belt in between the drum and the front sheet metal. Then I turned it on its side and worked the belt from the back hatch. I pulled the pulley back on the tensioner and slipped the belt under neath. Put it back together, been working great.
Parts Used:
Dryer Belt
  • John from Dushore, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Drum was not turning
This is the third time for a belt on this 28 year old dryer. Not too much to it. Unplug the dryer. Open the door. Remove the screws holding on the front panel and loosen the screw at the bottom. Disconnect the wires to the door switch and lift off the front panel and start up the shop vac to clean out the lint - there is a lot to be found in various places. Slide the new belt over the front of the drum and make sure there are no twists. You can now reverse the order to mounte the front panel but don't close the top so you have light to see inside. Go around to the back panel and remove the machine bolts holding on the access panel at the back. This allows access to the motor and belt tensioner. Get the shop vac out here and get to some more lint. Google the model number to find a diagram on how to route the belt. Put the belt on the motor shaft and around the tensioner as depicted. Occaisionally the plastic idler pully is worn and this can be the cause of the brokent belt. If the idler wheel does not spin freely, squeads or is cracked it should be replaced or you will be right back replacing the belt again. If all is fine it is time for a test run. CAUTION - you can plug the dryer in but keep your hands out of the cabinet as there are live exposed 220 volt terminals exposed. This allows you to observe that all is working and not binding during a test run with NO heat. If all is fine, unplug the dryer and put the covers back on. Reconnect the exhaust hose (now is a good time to clean that and the vent to outdoors as well).
Parts Used:
Dryer Belt
  • David from Dublin, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Dryer shut down completely, wouldn't start
Removed 3 torx screws on the control panel. Removed two more regular screws from the dryer opening. This allows removal of the top. Removed some panels from the back to access where belt feeds through the motor. Found the belt snapped in two inside.

Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.

Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
Parts Used:
Dryer Belt
  • Rob from Valencia, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Gas flame turns off after a while, dryer keeps turning but no heat is generated.
Before this fix which worked beautifully, I tried replacing the flame sensor which did not work. To read that story, search under part number PS459818 (Flame Sensor). Our model is a Westinghouse, so access to the unit is a bit different than the other stories. It's a stacked front-loader sitting on top of a washing machine.

1. Open the little front door (lower left side) by unscrewing the little screw right below it. The door will pivot and slide out vertically.
2. Disconnect the electrical main lead coming from the back of the unit (just in case).
3. Close the gas switch lever on main gas pipe coming from the back on left side (just in case).
2. Remove 2 phillips screws on top of the metal bracket holding the two coils. The screws have to be removed completely along with the bracket. It's easy, they are right in front and there is room for the screwdriver. Use a thin long one instead of one with multiple bits to better align with the screws, which are very close to the coils.
3. The two coils slide right out and are very different so it's easy to keep them straight. Remove electrical connectors before or after removing the coils (I marked the plastic on top with a sharpie to keep them in the right orientation).
4. Drop in the two new coils and reconnect them to the electrical leads.
5. Reconnect main electrical lead from back (match wire colors)
6. Reopen gas lever on gas pipe.
7. Drop in front cover at an angle, tilt vertically and put screw back underneath. Use magnetized screwdriver or a piece of scotch tape to hold the screw or it might fall off the screwdriver.
8. Voila'. It worked.

This website is great. Our dryer is a Westinghouse bought in 1991 (almost 20 years old!) and with this fix it's just like new. In 1994 we used parts bought here to fix our washing machine (Westinghouse LT350RXW1). That machine is now 15 years old and still going!
Parts Used:
M Series Ignition Coil Kit
  • Giuseppe from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
Parts Used:
M Series Ignition Coil Kit
  • Steven from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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broken belt
Took the top and front off. DO NOT TAKE DRUM OFF!! Lifted drum slightly and worked belt around drum. Replaced front and top. Took off rear panel at bottom near vent pipe. Put belt around motor and then tension pulley. Buttoned everything up and that was it!
Parts Used:
Dryer Belt
  • John from Perry, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
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Dryer Don't turn
I removed the 2 screws and lock assemblies from both sides on the back. Then i removed 4 screws (two from each side) on the control panel and lifted that up as i tipped the cover forward to disconnect the wires from the door switch. I found the wiring diagram inside the control panel cover, which included a belt routing diagram (very helpful, being the belt was laying in the bottom. I then removed 3 torx srews holding the drum to the bearing, and removed the drum. Let the fun begin! i proceded to put the belt onto the motor pulley and around the tensioner. i needed some help from my wife to set the drum back in as i held the belt up around it. once the drum was back in, i found the beld had fallen away from the tensioner. I lifted the front of the drum up just enough to get both arms below it and move the tensioner back to slip the belt over it correctly. With the new belt on i started to put the screws back in the drum. This got very frustrating, as you have to correctly line up all the holes again, while holding the drum in the correct angle to start the screws. this was the hardest part, not physically, but wears on a person's nerves quickly! Once all the screws were in and tight, i took a deep sigh of relief before i tipped the front cover up just enought to get the wires hooked back up for the door. I turned the unit on to verify the repair before re-assembly. Yep! works again, for well under $20.00! Thanks PartSelect!
Parts Used:
Dryer Belt
  • Matthew from Alma, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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No Heat
Removed gas line. removed control panel, removed top, removed front, removed burner, replaced igniter, put back in. paused and played the video. very easy to do. 42 minutes and I had a few beers.
Parts Used:
Dryer Igniter
  • Steve from Santa Ana, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
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Broken dryer belt on 30-year-old dryer
Found excellent instructions and diagrams online by searching under the model number. Best of all was the service from PartSelect. Belt arrived 24 hours after ordering. It was the right part, it was easy to install, and the dryer is running beautifully.
Parts Used:
Dryer Belt
  • James from Marco Island, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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loud noise when ran for 5 min.
Replaced the rear drum bearing. Not doing it before ,it took about 1 1/2 hrs. Problem was fixed.
Parts Used:
Rear Drum Bearing Kit
  • Joseph from Freeland, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Replace broken drum belt and belt idler pully wheel.
Watched video instruction, paying attention to what it showed in machine. Several virsions of similar designs over the years, look over yours and note access points, take pictures as you go! Just pay attention, it is very logical. Spread the side panels to get the drum in and out, and pay attention to drum axel in back and the bushing it rides in. Be patient, be firm but gentle, no real forcing needed if you are alligned. Be sure the grooves of belt are on the drum, drive wheel on motor, no twists. Reverse order to reassemble. There are several internet videos of models with same basic setup, so look at others if one doesn't show the detail you need to see, or clear some uncertainty. Your local hardware to sorce push fastening for the idler wheel to shaft if you mash it up, they are cheep and several styles will work.
Parts Used:
Idler Pulley Wheel
  • David from EASTON, CT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
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sqeekysqueeky rear drum bearing
Open top by removing 4 phillips head screws above opened door, pop top up. Remove rear access panel, remove belt from drive & tension pully. Loosen top front screws, remove front panel to gain access to remove drum. After drum removed, I realized why rear bearing went bad- two front guides were worn causing rear bearing to angle and wear out. Replaced front pads, buttoned her up and now quite as new. Also replaced drive belt while in there.
Parts Used:
Rear Drum Bearing Kit Dryer Belt
  • mitchell from Warren, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Dryer squeaked when running
Took the dryer apart to get to the rear bearing. Took the bearing assembly out, kept the e-ring from the old bearing shaft, replaced the bearing kit, took the o-ring off the new shaft and replaced it with the e-ring, then reassembled the unit. Make sure to place a nail or long screw into into the rear of the drum, so that you can realign bearing on the drum. It is easier with two people when reassembling.
Parts Used:
Rear Drum Bearing Kit
  • George from Dassel, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
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All Instructions for the CADG265RCL
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