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MLE19PDAYW Maytag Washer Dryer Combo - Instructions

All Instructions for the MLE19PDAYW
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Heat Would Not Come On
After replacing all the other fuses and sensors I finally replaced the Radiant Flame Sensor and it is working perfectly.

After replacing the other parts and the heat still not coming on I read somewhere that the Radiant Flame Sensor is a normal closed circuit and when I checked with a meter it was open. I would have saved a lot of time and money if I had read that earlier.
Parts Used:
Dryer Radiant Flame Sensor
  • Lynn from Novi, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
19 of 23 people found this instruction helpful.
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Daughters destroyed door seal with comforter caught in the door...
*** MY REPAIR STORY ***

*** Rule #1: READ THE OTHER STORIES FIRST! ***

The best tip was supplied by the guy that used a piece of good twine/string to help him reconnect the inner seal cable and spring assembly; the whole business of using a buddy to do so is a lot of hooey. Save yourself the aggravation of using your wife, kid or other mechanically-declined individual, and use the string trick. It is still a royal pain, but it is far superior with only one person, using the unbeatable mechanical advantage that the string gives you. I used a piece of good waxed poly twine; I tied it to a convenient hole near the front right side corner of the machine, and then threaded it throught the spring and pulled it with some good pliers in order to stretch the spring enough to re-engage the other loop of the inner seal cable, using needle nose pliers. Of course, it took about four shots to get it right, but I was particularly anal about getting the cable ends in their originally-installed orientation. In retrospect, it ought not make too much of a difference, as long as you keep the spring near the top of the drum and respect the placement of the cable: make sure it is fully in its recess in the seal, all the way 'round. Additionally, pay close attention to the drain hose attachment and outer seal installation; you don't want any more leaks. I have strong fingers so it was a snap, and there are both molded recesses, arrows and "tits" along the seal edges that correspond to the outline of the machine's mating surfaces. Please take the time to push in all the lugs all the way all around in all positions; your floor's dryness is depending on you. As far as the inner seal cable/spring situation goes, be aware that any slight failure to get it right will likely cause a "domino effect" that will necessitate that you to reinstall the seal along its entire periphery, on both inner and outer sides... hold onto that cable, and watch as you tension the spring... it will cause the inner seal to walk off the drum if you aren't paying attention, and you will not be able to recover the perfect position you had at first. In honesty, that is the only "difficult" part of the job. Ensure you've had ample food & drink before you undertake seal replacement ( and not alcoholic drink, either... ) !

As with all jobs of this type, the end was far better than the beginning... the machine doesn't spew water out onto the floor anymore, and helped reinforce my claim to the "most useful" Family Member status! lol My wife was nice to me for almost a week afterwards... your mileage may vary.

PartSelect.com, thank you so much for not only the right part at the right price delivered fast, but also the forum where others could report their repair experiences in order to give a good heads up to those contemplating this repair job. Super site, super business, would definitely use again. A+

Regards,

Glenn Buononato
Parts Used:
Bellow
  • Glenn from New Paltz, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
17 of 18 people found this instruction helpful.
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Rear Felt seal came out, squealing sound when drying
Turned off gas and unplugged dryer
1) Removed bottom front panel
2) lifted top panel up like a car hood
3) Removed door springs
4) disconnected electrial connections to door unit, removed door unit
5) removed drum, scraped old felt from drum
6) glued new felt with a very strong glue (nanoglue or gorilla glue, same thing), let it dry overnight
7) secured back inside panel, replaced drum and put dryer back together.
Parts Used:
Dryer Drum Felt Seal
  • Matthew from Lombard, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
19 of 24 people found this instruction helpful.
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Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!

NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Robert from Buffalo, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
17 of 20 people found this instruction helpful.
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Bad pressure switch on front loading washer allowed water level to exceed proper height leading to water leaking from door seal.
First I sent the local repair man away. I recieved much better advice from this forum. Partselect saved me literally hundreds of dollars. The local repair man was headed in the totally wrong direction.

After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
Parts Used:
Water Level Pressure Switch
  • Paul from Tallahassee, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
17 of 20 people found this instruction helpful.
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The spinner support had sheared off
First, I removed the drum. Removed the spinner support. Removed old seals. Reinstalled new spinner support. Reinstalled pulley and belt. Reinstalled drum. Reinstalled machine covers.
Parts Used:
Spinner Support and Seal Kit
  • Stacie from Las Vegas, NV
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
22 of 35 people found this instruction helpful.
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Washer would not drain
Starting out I found the code that the washer was showing,ND, Meaning no drain so I read up on and people where saying that the pump had a blockage in it, so I took the back of the washer to gain acess to the pump, I took the drain hose off to look in side to see if there was a problem there was nothing in the pump itself so I started to remove the pump I undid the wiring harness to find the problem, the red wire to the pump had burned in the harness order the part from part select and 30 minutes later my wife was doing laundry again..........Thanks partselect for the fast shipping and quality parts very easy repair.
Parts Used:
Drain Pump - 120V 60Hz
  • Scott from Sedalia, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
18 of 24 people found this instruction helpful.
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Dryer wouldn't start
We tried replacing the door switch first, still didn't start. Next we tried the thermal fuse and it turned on and has worked ever since.
Parts Used:
Thermal Fuse (Limit: 183)
  • SALLY from ANAHEIM, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
16 of 18 people found this instruction helpful.
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converted gas dryer to LP
Instructions were great. Very step by step. It could not have been easier. Repair saved me a $100 service call.
Parts Used:
Gas Dryer Conversion Kit - NG to LP
  • Bruce from Rogers, AR
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Wrench (Adjustable)
16 of 18 people found this instruction helpful.
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Bearings making loud rough noise
Thanks to all the others who gave detailed information I was able to replace the front & rear bearings and front seal. I must say it was a time comsuming job but at least I am alot clearer on the quality of clothes washing machines. I do believe I could give a manufacturer / designer some design points after working on this Maytag Neptune. I was able to knock out the bearing shaft that held the stainless perforated tumbler inside the plastic tub/drum by using a #3 LB hammer I reinstalled the old screw in the shaft which held the plastic pully on because this would keep the end of the shaft from being damaged. After several blows it started moving I was afraid I might damage the plastic drum but fortunately no damage was done to it. After removing the stainless steel perforated tumbler here is where it really got interesting. The Hub that held the old seal was shot! pretty much deteorated from corosion it seems. Here is where I could significantly help a manufactured/designer out The bearing/seal hub should have been made out of stainless instead of Pot metal/ aluminum or whatever they made it from. After much cleaning with a small wire brush and vacuming all the debree out of the Tub I didn't have much hub left to install the new seal. Also the three armed Spinner was very coroaded it attaches to the back of the stainless tumbler I removed it from the stainless tumbler and wire brushed it the back side was full of crud, it looked like left over washing powder or soap and Corosion debree it was a job just cleaning it up. I pressed on and on though replacing both bearings front and rear. Thanks to another person who explained the easy way to remove the bearings and race I was able to do so without removing the Drum/Tub as others stated they had to do. The Dremmel and a few Cutter blades did the trick I cut a wide V notch in the bearings and the bearings fell out I then cut through the bearing race being careful not to cut too deeply although if you did slightly cut beyond the race it really wouldn't matter because the front seal will keep it from leaking anyway. Anyway when I cut through the race it made a ping sound and the race pulled away and fell right out of the HuB. The front & rear bearings a definately serviceable and it doesn't have to be a beat/bang ordeal. after cleaning up the hub I tapped the new bearings in place and discarded the metal spacer that went inside the middle of hub. I then brainstormed on how I could install the new Lip Seal upgrade and then it dawned on me that since the inner Hub that holds the seal was so far gone and only enough left to barely hold the new seal in I remembered the ole saying Don't Discard just use JB Stick or JB Quick I used JB Stick to fill in around the new seal because it is supposed to bond to metal and it did just that I pressed the putty in quickly before it hardened bringing it out even with the plastic drum where the origional hub should have been and made the repair to the deteriorated Hub so that the Seal would stay in place it Worked! This Maytag Neptune was given to me by my mother in-law she did not want to wait on the repair after I tried to previously repair the problem with it I just did not delv deeply enough into the problem with this washingmachine at first. I previously removed both Pumps thinking they were not pumping all the water out because the Towels especially were staying soaked. Both the pumps were nasty with alot of debree inside of them now I know that because of the deteriorated Seal Hub on the inside had done the dirty work. The Pumps can be easily taken apart only a few screws and the plastic impeller can be gently pried off also that is where I found alot of particles from the deteoriated Seal Hub I then reinstalled the pumps and they worked fine pumped out the water. Then that is when I noticed it wasn't cycling properly also Ha Ha I thought to myself what else could possibly be wrong with this washing machine? Thanks to Parts Select site I wa
Parts Used:
Lip Seal Kit
  • Gregory from El Dorado, AR
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
17 of 22 people found this instruction helpful.
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LR Code on the display, washer would not spin.
Removed the front panel and took out the old control board, which had a burnt spot on it. Removed back panel and took out the old motor. Put in the new motor and then the new control panel. Runs perfect.
Parts Used:
Motor and Control Board Conversion Kit
  • William from Colver, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Wrench set
18 of 25 people found this instruction helpful.
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the problem is the motor
first i follow the instruction come with parts in box...and replace easy this the best place to buy parts for all home appliance...thanks
Parts Used:
Motor and Control Board Conversion Kit
  • Bick from Alameda, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Wrench set
19 of 29 people found this instruction helpful.
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Time clock not moving .Not enough heat
Opened front panel .Tested both coils on gas valve.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
Parts Used:
M Series New Style Coil Kit
  • PHILIP from LONG ISLAND CITY, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
16 of 21 people found this instruction helpful.
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broken clip for door latch
popped out old female clasp on dryer itself with screwdriver, undid 2 screws on dryer door and door handle with phillips screwdriver, popped in new male clasp part, put door knob back on and put the two screws back in door and it was all set to go. Less than 15 minutes to do. Better than new and wife is happy. No more duct tape holding door closed now.
Parts Used:
Door Latch Kit
  • Shawn from Dover, NH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
14 of 15 people found this instruction helpful.
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loud noise inside dryer
After changing all the rollers in the dryer (which didn't fix the problem) I decided to take apart the blower. Sure enough, that was the problem. As the dryer heated up, the damaged wheel would swell and start rubbing the housing. I replaced both and fixed the problem. The repair was pretty easy, since I had taken the dryer apart several times replacing the rollers.
Parts Used:
Blower Wheel Blower Housing
  • Terry from Caruthersville, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
15 of 18 people found this instruction helpful.
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All Instructions for the MLE19PDAYW
61 - 75 of 992