Models > VGD6505GW0 > Instructions

VGD6505GW0 Crosley Dryer - Instructions

All Instructions for the VGD6505GW0
31 - 45 of 637
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Door Gasket tore out
Put high temperature glue on first, then put door gasket over the high temperature glue and then let it set for 24 hours. It worked fine....
Parts Used:
Door Gasket
  • Manolak from MURFREESBORO, TN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
15 of 15 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.

Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.

While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.

Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:

I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.

The drum was set on the seal and rollers at the back of the dryer.

The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.

The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.

The new belt was then gently installed under the temporary support rope and around the drum.

The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.

Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.

With the belt attached, the temporary cardboard shims were removed from under the idler pully.

The front of the dryer was attached .

The temporary board and rope hanger was removed.

The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.

The seals as well as the remainder of the dryer assembly was completed without any problems.

The dryer ran well for its initial trial spin and has dried several loads of laundry since.

Great parts and support Thankyou
Parts Used:
SEAL Lint Trap Housing Seal Multi Rib Belt - 92-1/4"
  • Benjamin from WELLS, ME
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
15 of 16 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dead motor
1. Shut off gas and disconnected dryer.
2. Opened cabinet. Easy sheet metal screws and fairly obvious how everything goes together. NB: You'll need a block (or a helper to hold things while you run to look for one) to hold the drum while removing the front.
3. The motor is connected with a single harness, so wiring is a snap.
4. Removing the blower wheel from the back was hard. I braced the motor shaft and turned with all the leverage I could muster, but it was stuck. Plan B: Recip saw to cut the shaft. Motor comes out one side and the fan comes out the other.
5. The fan, of course, was unusable because there was still a piece of motor shaft stuck in the thread. This is why I had to spring for a new wheel.
6. Put everything back together and receive wife's adoring praise...
Parts Used:
Dryer Blower wheel
  • Robert from Glencoe, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
17 of 24 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Change dryer belt
I opened up the dryer as per the instructions I had received from PartSelect tech support. It was very easy to do. The only unexpected thing was that the original belt had snapped and in doing so the idler pulley was actually laying on the floor of the dryer's bottom. I had to figure out how it went, but that only took a minute and I popped it back into place. I held the drum by hand while pulling the dryer face away so it wouldn't fall and then I slipped the belt over the drum and quickly closed the front up again. I aligned the belt on the spot where the old one had been, pulled it through the idler pulley and over the motor and voila. Done. I closed up the dryer and was on to another "Honey Do" project within 20 minutes.
Parts Used:
Multi Rib Belt - 92-1/4"
  • Scott from Bayport, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
14 of 16 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
the drum was not turning because a broken belt
I lifted the top of the dryer cabinet, like the hood of a car using a screwdriver to pry it open. I removed the two screws in the upper right corner of the cabinet front. I disconnected the safty switch on the front door. The front of the cabinet can then be removed by lifting up the front off the pins in the base. With the drum exposed you can place the belt on and thread it through the two pulleys on the motor. Consult the diagrams provided on the PartsSelect website for the proper positioning of the belt on the pulleys. After the belt is installed spin the drum by hand one turn to make sure that it is seated properly on the drum and pulleys. Reassemble the dryer in the reverve order.
Parts Used:
Multi Rib Belt - 92-1/4"
  • thomas from bloomfield, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
14 of 19 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Aft seal deterioated and causing brown spot on clothing due to netal to metal contact.
Removed top and front of dryer then drum and followed the instructions in the package. It was a real simple procedure. I did additional cleaning while the dryer was disassembled.
Parts Used:
Rear Drum Felt Seal
  • Cleo from Laurinburg, NC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
11 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
dryer would stall and the motor would hum before tripping circuit breaker
When the problem first came up, I took the dryer apart without first looking up any instructions. This wasn't difficult, but didn't realize when removing the fan from the motor, there is a square lug as part of the fan hidden by the rear clamp securing the motor. I was able to remove the fan by holding the motor shaft with a crescent wrench and removing the fan by hand, but was difficult and gloves were necessary in case the fan loosened quickly and my hand came in contact with the sheet metal (very sharp).

I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.

This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.

The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
Parts Used:
Drive Motor with Pulley
  • Charles from Placentia, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
11 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
My dryer handle broke off when i opened it
My son got it in the mail for me and snapped it right back on.
Parts Used:
Dryer Door Handle - White
  • Kathy from CORNING, IA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
12 of 15 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The handle to my dryer broke
Just popped it into place needing no tools at all. Took less than a minute.
Parts Used:
Dryer Door Handle - White
  • Elouise from ORLANDO, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
10 of 11 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Had to convert from natural gas to propane
Well, here's the rub...in order to find out what part I needed to order, I needed to take the dryer apart to where the gas controls are, and there on a sticker was a part number for an LP conversion kit. But, in order to get to that gas valve unit, I fumbled about figuring out how to take this brand new dryer apart, since there were absolutely no instructions whatsoever in the owners manual. And once apart, and pretty much all apart, I wondered how it would be that the Maytag repair man would be so lonely, as he'd have plenty to do.
However, the kit had great instructions as to how to take it apart and change out the orifices.
Parts Used:
Liquid Propane Conversion Kit
  • Peter from The Rock, GA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
12 of 18 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
LP gas conversion
Followed instructions, except to advoid sharp edges, and completed the job in under an hour.
Parts Used:
Liquid Propane Conversion Kit
  • Robert from Palmdale, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
11 of 15 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
Parts Used:
Multi Rib Belt - 92-1/4"
  • Ronald from Oakdale, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
10 of 13 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Old motor was making noise and tripping after a few minutes
I disassembled the dryer once to clean the motor and compartment. After reasembly, the problem persistes. I ordered the motor and the second diasasssembly was accomplished in 10 minutes and the entire job took 45 minutes and the dryer was running like new. Tip- Leave the motor secured while removing the blower fan.
Parts Used:
Drive Motor with Pulley
  • John from Midland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
10 of 13 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
A piece of cloting snagged and broke the door switch.
Repair job took less than 10 minutes: 1) Unplug Dryer 2) Remove Lint screen and 2 Phillip screws 3) use flat putty knife to depress lid latches while lifting (latches located approx 2 - 3 inches from each side. 4) unplug defective door switch 5) remove 2 Phillip screws that secure the door switch. Reinstall switch repeating the above steps in reverse order and your done.
Parts Used:
Door Switch
  • Ronald from LANCASTER, CA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
9 of 10 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Humming noise then quit after pushing start. Drum would not turn manually.
Looking at the schematics, it wasn't clear exactly where the motor was located. I took off the rear panel thinking I could get to the motor through the blower. Realizing that was a no-go, I did some web searching and found that the lint screen chute had to be unscrewed, the top had to be lifted to gain access to the top 2 screws holding the front panel to to the main body. The barrel was then dropped and the rib belt removed from around it so I could set it aside. The clips were removed from the front and the back of the motor to gain access to the blower shaft. .The motor shaft is screwed into the blower shaft but it took me a while to figure out how to grab the blower shaft( made of hardened plastic?) with an adjustable wrench while torquing the end of the shaft with a (3/4"?) socket wrench. Access to the rear was rough, but getting the motor out an back in was easy. The spring tensioner for the belt was the next hurdle. With the s-curve facing outward and clipped to the base, the belt with the rib side wrapped around the barrel, the belt was slid between the roller and the tensioner bracket and wrapped around the motor drive rib side inward. I had to take the old motor to kind of prop up the barrel so I could at least see the tensioner and motor interface. I had to do a balance trick where I held the barrel up while centering it to the belt and the rear panel while ensuring the cloth seal was seated to the outside of the chamber. The front panel went on, and the front cloth seal was seated by spinning the barrel. The rest was just a matter of reversing the steps. Tons of lint/dust is probably what crashed this motor. Disassembling the front and the back allowed a thorough clean up - vacuuming and wipe down. Should go another 10 years/
Parts Used:
Multi Rib Belt - 92-1/4" Drive Motor with Pulley
  • Derek from Missouri City, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Socket set, Wrench (Adjustable), Wrench set
8 of 8 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the VGD6505GW0
31 - 45 of 637