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MLG20PRAWW0 - Instructions

All Instructions for the MLG20PRAWW0
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Door Catch was broken
I just inserted the door catch, which by the way fit in perfectly. Thanks. Took 5 seconds to repair.
Parts Used:
Door Catch Kit
  • Inocencio from Edinburg, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
15 of 16 people found this instruction helpful.
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motor would not stop at end of cycle
Remove compactor drawer
Remove screws holding compactor to counter
screw in adjustable feet a short distance
slide compactor out far enough to unplug
loosen top screws that hold tiedown strips and move tie down strips out of way
remove two phillips screws on control panel
push control panel assymbly up and out of front of compactor
remove and replace wires one at a time onto new switch
remove two phillips screws on old switch and removeswitch.install new switch with same screws
install front switch assy by inserting in front panel of compactor and pushing down untill two holes match up for phillip screws.
install screws
realign both tie down straps and tighten screws
plug in compactor
push compactor back into place
level compactor with adjustable feet
replace tiedown screws to underside of counter
replace compactor drawer
push on/off switch to on. push start switch to start compactor.
watch as compactor stops at end of cycle. Hurrah!!
Parts Used:
SWITCH-OFF
  • John from Sandy, UT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
17 of 23 people found this instruction helpful.
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seal for lint filter came off
Pulled out the old and slid in the new filter
Parts Used:
Lint Filter
  • John from Midland, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
17 of 23 people found this instruction helpful.
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Time clock not moving .Not enough heat
Opened front panel .Tested both coils on gas valve.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
Parts Used:
M Series New Style Coil Kit
  • PHILIP from LONG ISLAND CITY, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
16 of 21 people found this instruction helpful.
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Flashing E1 code for a bad thermistor
I replaced the thermistor earlier, but the code was still flashing. I noticed the heater terminals were charred and pretty well covered in carbon. So, I replaced the heater, the thermostat and thermal fuse and replaced the 3/8" spade terminals on the heater wires. (These are hard to find - most electrical spades terminals are .250. Also, I crimped and soldered these for a connection with the lowest resistance possible). After all that, the code still flashed! I let the explatives fly, calmed down, and ran the control board test. (This is done by pressing "more time" "less time" "more time" "less time" in succession.) The control board was passing all the tests, but the thermistor test, and the only thing is in this circuit is the thermistor, the wires, the connector to the control board, and some circuit on the control board that involves a few resistors and the "brain" chip. So, I checked the terminals at the thermistor, the wires up to the control board and the connector at the board. The control board connector was fairly dust encrusted, so I unplugged it, cleaned the control board terminals and sucked away all the lint and dust. Finally, I carefully removed earch crimp terminal from the Molex connector (the white female connector) and cleaned and bent them to yield a better connection to the terminals on the control board. I put it all back together, and thus far it is working fine.
Parts Used:
High Limit Thermostat and Thermal Cut-Off Kit
  • John from Cedar Rapids, IA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
17 of 25 people found this instruction helpful.
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Dryer gasket detached from screen
Received in two days, open box, installed part. Pretty easy, fast service. I'm a repeat customer and will use these guys in the future.
Parts Used:
Lint Filter
  • Richard from Duarte, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
14 of 17 people found this instruction helpful.
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Burner would not go on on my Stack Set Dryer
Took out two front Panel screws and removed the panel. Removed Gas solenoid coil holding bracket by removing two phillips head screws. Disconnected the coil leads. and removed the coils. Connected the new coils to the leads and set in place. Replaced the holding bracket and the two screws. Replaced the front cover and the two front cover screws. Piece of Cake!
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Robert from North East, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
16 of 24 people found this instruction helpful.
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The Dryer would not get hot.
I removed the two screws holding the access panel, and removed the access panel. Then removed the lower air duct. I then checked the burner, The solenoid was not opeing the valve for the gas. I order the coils, in two day I had the coils and installed them. The dryer is working great.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Jerry from Bradenton, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
14 of 20 people found this instruction helpful.
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Would not drain
Removed bottom panel, removed hoses and pump. Reinstalled in reverse order.
Parts Used:
Washer Drain Pump
  • Tammy from Maryville, TN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers
14 of 20 people found this instruction helpful.
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The dryer was not fully drying
After replaceing several parts including the thermostats the last part I replaced the coils were the defective part. I originally metered out the themostats and they appeared to be okay but since this was my first time I thought I might have been mistaken. It turns out the last part I thought it could be was the part that was defective. I will say that it is very simple to replace any of the parts involved. The hardest part was trying to open the dryer itself. But after having to do it 3 times, I'm now a pro. I also replaced the drum belt and since I had it open I also replaced the belf idler with a newer modified idler rolller.

Putting the belt back on is easy, but it helps to view the video or a picture to understand how the belt goes around it.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Michael from Chicago, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
12 of 14 people found this instruction helpful.
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dryer not heating up
Unscrewed 4 screws,pulled off front of machine.Unscrewed 2 screws holding coils on,unplugged coils,installed new coils,plugged in coils,reinstalled 2 screws for hold down brace.Reinstalled front cover,plugged dryer into outlet(remember to unplugged dryer before working on it).started up,instant heat,works great.thanks Partselect for helping me out!!!
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Richard from New Windsor, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
12 of 14 people found this instruction helpful.
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Rear dryer drum seal came out
Used my Whirlpool Dryer User Instructions Manual and followed instructions and used the Cabinet Parts page to see the diagrams.
Parts Used:
Dryer Drum Seal with Adhesive
  • William from Pontiac, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
16 of 28 people found this instruction helpful.
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When using the dryer the cycle would stop and display E1 as the reason
Unscrewed the bottom panelof the dryer and located the thermistor through the schematic for my machine. Removed the old one and put the new one in the same way. No more E1 problems and all cycles now complete themselves.
Parts Used:
Thermostat, Internal-Bias
  • Joyce from Holbrook, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
12 of 17 people found this instruction helpful.
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
12 of 18 people found this instruction helpful.
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
10 of 12 people found this instruction helpful.
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All Instructions for the MLG20PRAWW0
46 - 60 of 471