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DBLR333EEC General Electric Dryer - Instructions

All Instructions for the DBLR333EEC
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Low heat
Checked the fuse box to see if any breakers tripped on the two 120 lines feeding the dryer.

Checked for clogged exhaust vents/hose/etc, cleaned.

Some paint flaking off inner drum around heat vent.

Unplug & disassembled unit. Took pictures for reference to help with reassembly later. Upon removing drum, found sagging heat coils, one broken, some heat damage to the housing near the top. Determined that more than just coils needed replacing.

Also checked each of the three heat sensors (cycling thermostat, high limit thermostat & safety thermostat) with the digital multimeter. All were positive continuity for low temps.

Tested ONLY the cycling thermostat on the kitchen stove with burner set to warm. Check burner temp with meat thermometer to see it exceed 120F. Continuity broke at high temp. Although the cycling thermostat seemed ok with my generic test, I decided to replace it anyway.

My understanding of the Safety Thermostat & High Limit Thermostat is that they work like safety fuses, breaking at dangerous temps, but not resetting afterward. So these were only tested at room temperature, not with heat.

With the unit open, I checked other components for signs of wearing out. Also cleaned the unit more thoroughly.

Reassembled in stages. The belt is the trickiest part to get back on the motor & tension pulley, it's just a little awkward to reach. Tested to make sure the drum moved freely and belt was correct before finishing the reassembly.

Checked to make sure the dryer was still level, after all the moving around, disassembly & reassembly.

Ran several supervised test loads. Felt the temperature. No tripped breakers or smoke. Exhaust was flowing unhindered. Clothes got dry.
Parts Used:
Cycling Thermostat - 4 Wire Heating Element and Housing
  • Jaeson from STATE COLLEGE, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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slides worn and belt broken
Unplugged power. removed 2 screws to take of top cover. once inside removed 2 more screws to slide front panel of. I first replaced slides on front panel. I then lift drum and installed new belt. Only trick is to make sure you wrap belt around tension arm pully properly. Basically a very easy job
Parts Used:
Drive Belt Drum Bearing Slide - Green (Sold individually)
  • Mark from salem, NH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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no problem
this was a part i ordered for future use. i was very happy with the ordering process and speed of delivery from PartSelect.
Parts Used:
Lint Filter - White Frame
  • john from west milford, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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remove plastic and insert
inserted the lint catcher into the opening to replace the old one
Parts Used:
Lint Filter - White Frame
  • MARY from ERIE, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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loud screeching and long dry times
When we first heard the screeching i thought right away that it was the belt. we ordered a new one and after i replaced it the dryer was still just as loud. I wished i went here first. Right away i found others with the same problem, did the same repair which was just taking 2 screws out, sliding the top and front panel off(watch for the electric wire connected to the panel) and replace a couple of plastic slides. now it is better than ever.
Parts Used:
Drum Bearing Slide - Green (Sold individually) Drum Bearing Slide - White (Sold individually)
  • Brad from Batavia, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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My dryer was making a really loud, high pitched squeak and eventually a grinding noise
I order the parts needed to replace the slides, the felt ,and the bearing on a Sunday afternoon. The parts arrived on Tuesday even though I used regular shipping. I followed the instructions posted by another customer. It was extremely easy and only took me about fifteen minutes. My only problem was that I needed 2 each of the front slide and the rear slide, and I unknowingly only ordered 1 of each. I order the other 2 on Tuesday via regular shipping and they arrived on Wed. AMAZING!!!!
Parts Used:
Drum Bearing Slide - Green (Sold individually) Drum Bearing Slide - White (Sold individually)
  • Amy from Round Pond, ME
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Loud noise
First I watched the repair video on partselect.com and that really helped. It was really easy to replace the slides. I even ordered a new top bearing, old one was busted, and replaced it. Thank you for your help.
Parts Used:
Drum Bearing Slide - Green (Sold individually) Drum Bearing Slide - White (Sold individually)
  • Phillip from Kissimmee, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Dryer belt was broken
I removed the top cover and the back cover to install new belt.
Once i put new belt i discovered that the pulley was also broken so now i have order the pulley so that i can complete the repair
Parts Used:
Drive Belt
  • Alvino from newtown, CT
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Rythmical Squeaking
The instructions that came with the bearing were limited and the illustrations were too dark to see. However, after reading the reports of others on this website, the repair was very easy.

Prior to disassembly, remove theaccess panel on the rear of the dryer. Pull the belt drive pulley arm up and the belt will easily slide off of the motor pulley. The belt can be left on the drum.

Then, remove two screws at the inside top of the dryer door. The top of the dryer will then lift up at the front and slide forward to remove. This will allow you access to two bolt head screws on each side of the front panel. Remove these two screws and then lift the panel slightly up and forward. The front panel will then be free and the dryer drum will slide forward and out. Remove the four bolt head screws (behind the electric elements) from the heater element on the inside back of the dryer box.

You can now exchange the bearing on the drum and the bearing insert on the dryer heating element simply by removing the old and reinstalling the new just as the old was removed - four screws for each.

You will need an assistant to re-install the bearing. Someone needs to hold the three pieces behind the drum as you insert the three screws. You'll also need a star wrench set for this.

The drum is easily reinserted - just be careful to get the front of the drum placed into the front bearing surface when reinstalling the front panel. One word of caution, My wife tried to remove the felt bearing on the bottom of the front panel thinking that it was lint.

I found that the inside of my ten year old dryer was unbelievably full of lint. I'm sure that the efficiency improvements by cleaning the air passages will be substantial and I've just saved $400 on the price of a similar dryer ($900 if my wife and I decided to upgrade to the "new" model that we wanted but really didn't need.
Parts Used:
Rear Drum Bearing Kit
  • Michael from Edmond, OK
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Very loud squeak with drum rotation
Key starting point is to remove top cover by removing two long screws located at the front of the cover
Remove control panel and it's bottom and side supports.
Remove short vent pipe by bending retainer tab.
Support the drum at the top using piece of rope.
Remove main rear cover (leave bottom attached).
Remove electric heating unit and install new bearing carrier from kit.
Reinstall the the heating unit
Remove three screws (inside the drum)to release the inner drum cover and release the bearing carrier.
Install new bearing carrier. Note: the three holes in the bearing carrier are not tapped, I suggest that the screws be installed (threads cut) into the bearing cover before attempting to install the bearing carrier.
Install the new bearing carrier. Note: pilot one of the holes using a small nail etc. then go on to install screws in the other two holes remove the pilot device and install the third screw.
Reassemble in reverse order.
Parts Used:
Rear Drum Bearing Kit
  • William from San Juan, TX
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Wrench set
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The timer knob was cracked and the metal "D"-Ring was broken on my GE cloths dryer
This repair was a no brainer repair. The factory replacement knob that I bought from this site comes with a new "D"-Ring. Some other aftermarket parts houses sell the knob and the "D"-Ring as seperate parts. The knob from this site already has the "D"-Ring ring installed in the knob. My "D"-ring was broken and I simply removed it with my fingers. All I had to do was properly align the new know knob with the timer shaft and press it into place. If your "D"-ring is not broken and not still inside the old knob, you will need to pull it off the shaft with a pair of pliers before pressing the new knob onto the timer shaft. Dr. "B" The Hot Rod Doc
Parts Used:
D-Shaped Knob Clip
  • Lynn from MORGANTOWN, WV
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
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belt broke
had a great video to follow, made it easy to install.
Parts Used:
Drive Belt
  • joseph a from VALLEY STREAM, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
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Dryer's drum doesn't run
Follow YouTube "how to change dryer's belt" some video is very clear.
Parts Used:
Drive Belt
  • ruoli from Germantown, MD
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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thumping noise with any kind of load
looked at video of dryer disassemble, replaced 4 bearing slides, reassembled. Dryer is perfect now , no noise. thank you for your parts.
Parts Used:
Drum Bearing Slide - Green (Sold individually) Drum Bearing Slide - White (Sold individually)
  • John from SONOMA, CA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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All Instructions for the DBLR333EEC
76 - 90 of 329