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11088732790 Kenmore Washer Dryer Combo - Instructions

All Instructions for the 11088732790
61 - 75 of 1877
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Tub was out of balance
went by the instution in the box with the part went very well thanks
Parts Used:
Tub Spring Suspension Spring - Kit of 3
  • Delbert from Morgantown, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
26 of 38 people found this instruction helpful.
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valves allowed water to overflow during the rinse cycle, sometimes took forever to fill.
I removed the screws holding the control unit down, removed a couple at the rear,
Disconnected the electrical clip that plugs into the top, under the control unit.
This allows enough slack to pivot it ( the control unit) upside down and get it out of the way enough to remove the spring clips that hold the top to the back.
Popped out the two clips that hold the back to the top.
Pulled the back out, up until the plastic soap dispenser , (which is attached to the back) hits under the lip of the top.
This does not allow enough room to get to the valves.
I finally figured out you have to lift the entire top up high enough to clear the back while pulling it ( the back) out.
Disconnected the hose clamp, electric connectors, installed the new valves into the supplied mounting plate replaced the valves .
Re -connected the hose and electric connectors and re assembled the back.
The only problem I had was when one of the spring retainers that hold the back to the top popped off and fell inside the unit, which forced me to remove everything including the back bottom screws, which caused the sides to pop off, the mounting ears , which are attached to the back,
Took some finesse but finally retrieved the spring clamp and finished everything back together.
It was a bit tricky keeping the plastic gaskets between the back and the sides from falling inside as I reassembled it.
But all is well, and would have been more difficult without the expierence written by others who posted, on the site.
Thank you to all, for the help.
I hope my efforts will help someone else.
Parts Used:
Water Inlet Valve with Mounting Bracket
  • Sam from Robertsville, MO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
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Push start and the motor would hum.
**** Remove power cord from the wall****

As said earlier, you will need to lift the top. Drop the two screws holding the lint shoot and pop the top by sliding a screw driver into the corner on the front. Lif tthe top and rest against the wall behid the unit. remove the two (4 total) screws at the top and bottom of the front door assembly.
Place sometin under the front portion of the drum. At this point you'll see the need to clean everything! :) Slide the belt off and around the drum, (take note of the routing it takes.) Remove the drum by gently pulling it towards you. Set it aside. Clean more. :) (It is nice to have a vacuum handy.) At this point you really need to get to the rear of the system. So I tipped the top back down, and spun it around. Removed the rear panel and cleaned some more. (15 years of a lot of lint in there!) Then you'll need to remove the rear cover on the left side, covering the blower impeller. Get read for a whole lot of debris. Vacuum again. So now you have the motor exposed in the front and rear. You need to remove the impeller by turning that clockwise to loosen it. The trick is holding the shaft in place from the front at the same time. I used an old rag and wedged it into the impeller edges and worked it around until it jamed up. Once the rag was wedged pretty good, I went back to the front spun the shaft. Then you can remove the impeller by hand. Vacuum more. You may get by without having to remove the lint shoot completely, but I did just to clean it up more. I did have to remove two screws in the upper corner near the top of the lint shoot. (Basically the hold the back in place.) I took a few notes at this point about the wiring harness. Used a heavier screw driver (standard), You can push down on the clips that hold the old motor in place. Then work it out the front. Clean more. The new motor is not an exact replacement slightly differnt but the instructions with it were ok. Follow them for the correct wiring. You will need to remove one wire and cut and recrimp a spade lug or two. I used ty-wraps to secure the lines back in place. Look closely at the diagrams and make sure you set the motor down in the same direction the instructions say, if you twist it slightly it will sorta lock in place where it needs to be. Re-install the hold down clips to the front and rear of the motor. Clean up your impeller, and reinstall it too. Then basically reassemble the dryer...tracing your steps backwards. This isn't really difficult, it just takes time and as you can see, you will/should clean as you go !
Parts Used:
Drive Motor with Pulley
  • Doug from Manitowoc, WI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
22 of 26 people found this instruction helpful.
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In the middle of changing loads there was snapping and sound and drum stopped turning.
I was hopeful it was the belt. But, I had no idea how to get to it. I used the model no. and looked on line for pats and schematics. That gave me a sense of what to do. I started at the rear and removed the back panel. It was like peeling an onion because then, I wasn't sure what to remove next. So I just kept removing nut head screws until eventually I had loosened the sides, removed the top and discovered the front lifted up and off (no screwed attachment.) There's grounding wire that must be detached. Don't forget to re-attach. Without proper grounding you could be electocuted! I was careful to remember how it was attached. To get to the pulley, which is on the front, I had to remove the drum. I found the snapped belt. The pulley is held in place by tension from the belt so, once the belt goes the pulley detaches. I tried to find the belt locally the following week but was unsuccessful. I found the part on-line and had it in four days. It was tricky getting the belt and pulley in place. I persevered.
The parts ( I replaced the fliter that needed replacement for years too) came with installation instructions. Its possible I did not have to disassemble as much as I did. Oh well! Although I'm fairly mechanical, I'm still pretty proud to have been able to do it and save the cost of a repairman.
Parts Used:
Dryer Lint Filter and Cover Multi Rib Belt
  • William from Glen Burnie, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Socket set
23 of 31 people found this instruction helpful.
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The spin gear was striped.
I had to take the motor and transmission out. They are one piece. Removed the clutch, take off trans. cover, remove a snap ring, take the striped gear off, and put the new one on. Then put put everything back on the way it came off.
Parts Used:
Gearcase
  • Aaron from Lake Mills, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Socket set
21 of 27 people found this instruction helpful.
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The Dryer Would Not Turn On
The dryer wouldn’t turn on at all. It was like it was unplugged from the wall. However, fixing it couldn't be easier. I simply removed the back panel, found the fuse, tested it with an Ohmmeter (to determine that this was the part that didn't work), ordered the part from this website, and replaced the part. The part arrived in about two days. The shipping was a little pricey, but overall the whole thing cost me $20 vs. whatever it would cost me to get someone else to repair it. The website helps to identify the problem, and it is helpful to read how other people fixed their problems. It was so easy and the service was so good, I will definitely use this website again and recommend it to others.
Parts Used:
Dryer Thermal Fuse
  • Ribhe from Wildwood, MO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
18 of 18 people found this instruction helpful.
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Although the motor was running, washer wouldn't agitate or spin.
After disconnecting the electrical supply, first remove the two screws at either end of the control panel and fold it back away from the washer top. Then, unplug the electrical lid switch connection. Now, remove the two clips at either end on top to disconnect the housing from the washer back and chassis. The motor is sandwiched between the water pump in the front and transmission at the rear. The Direct Drive Coupling connects the rear motor shaft to the transmisson. After you have taken the outter portion of the washer off, remove the two snap clips that hold the water pump in place and slide the pump off the front shaft. Best to also disconnect the upper hose connection so the pump can be moved out of the way. Caution though, remaining water in tub will drain out. Now remove the two screws that hold the clips in place which secure the motor to the transmission. Careful, as the old Direct Drive Coupling is probably destroyed, the clips are the only thing holding the motor in place and the motor needs to be supported so it won't drop to floor when the clips are removed. Be careful not to lose the four rubber grommets which sit between the motor and transmission bracket. After motor is on floor remove the old plastic slip-on direct drive coupling discs from both the motor and transmission shafts. The new replacement discs have steel centers which do not slide onto the shafts as easily as the old plastic ones did. I had to tap the center steel portion onto the shafts using a hammer and a deep wall socket the same width as the steel portion of the disc. Be careful! I'm sure that tapping the plastic portion of the disc to properly seat it on the shaft will break it away from the steel portion. In my case, It took me several attempts to completely seat the new discs. I had to do quite a bit of tapping to get the discs seated far enough onto the shafts so that the motor slipped easily against the transmission bracket grommets and the retainer clips snapped back into place easily. Reassembly is simply reversing the steps you took when taking the unit apart. Before putting the outter housing back in place, I checked to make sure everything was running smoothly by jumping out the electrical snap-in connection for the lid switch and running the machine in the spin cycle. Remember, if you don't jump out the lid switch and just try to test the unit in the aggitate cycle, the machine has to first fill with water.
Parts Used:
Direct Drive Motor Coupling
  • Thomas from Commack, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
20 of 24 people found this instruction helpful.
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Dryer drum would not stop spinning when door was opened
This dryer is a stackable washer/dryer. I removed all the buttons on the front panel along with the panel. I then was able to lift the front of the door and reach in to the door switch and plug. I unscrewed the old part, installed the new one. I then put the front panel and face plate back into position and screwed them back to the dryer casing. Lastly I put the knobs back on. I was extremely impressed at how easy it was to order and how quick the part came to my house. I am very satisfied with the service and the price and will use this site again in the future.
Parts Used:
Door Switch
  • Debra from Clarksburg, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
26 of 43 people found this instruction helpful.
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Drum was binding because of worn bearing supporting front of dryer drum
First I unplugged the dryer for safety, then I removed the top of the dryer, then removed the 2 hex head screws holding the font door panel onto the dryer. Then I disconnected the door safety switch. the rest was cake. I removed the old bearing and cut the new bearing and seal to the exact size of the old one. I used contact cement to glue the new bearing and seal into place. Reassembly was a breeze. End of job. Success!!!
Parts Used:
Bearing and Seal Kit
  • Leslie from Townsend, GA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
22 of 33 people found this instruction helpful.
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Top Half of Agitator would not function without appying sideways pressure
Heard about the website... 1 minute to find it, 10 minutes to order new cogs... 3 day wait for new parts... Rec'd Fedex, 15 minutes total to pull the agitator cover (bleach dispenser) then the bung cover with o-ring (just lift out) expose bolt, unskrew and remove top portion of agitator or entire agitator if it's easier. Seperate, remove black cog holder (slides up the spindle) and replace cogs one at a time just like the old ones. Reassemble in reverse and you are back in business. Saved the $75 deductible on my home appliance warrenty. You guys are the best... cheers...
Parts Used:
Agitator Directional Cogs
  • Donald from Fredericksburg, VA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set
18 of 21 people found this instruction helpful.
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Agitator was barely agitating. Making a clicking noise.
Removed agitator cap. Removed bolt inside with socket wrench. Located plastic cogs Pulled out old cogs and slid in new cogs and put back together and works great. Easy to take apart and put back together. Very cheap repair. Cogs less that $4.00 plus shipping. Shipped next working day.
Parts Used:
Agitator Directional Cogs
  • Charmaine from Slidell, LA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set
17 of 18 people found this instruction helpful.
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The movers broke both water intakes off flush with the back of the machine
took off two screws that held the top part on took the screws that held the back on 4 screws removed the one screw that held the replacement valve put the black mounting plate on the machine replaced screws very simple.
Parts Used:
Water Inlet Valve with Mounting Bracket
  • Dennis from Oak Island, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
16 of 17 people found this instruction helpful.
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Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!

NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Robert from Buffalo, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
17 of 20 people found this instruction helpful.
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Water was leaking at the pump
Actually this is kinda funny. I ordered the part and it arrived when I was out of town on business. My 20 year old daughter tipped the washer up on its end, and replaced the pump herself in less than 30 minutes. Her only complaint was that no one told her to block the washer up as it almost fell on her.
Parts Used:
Direct Drive Water Pump
  • Paul from Painesville, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
17 of 21 people found this instruction helpful.
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Would not spin
Remove the nut from the top of the motor shift inside of wsher. then remove the wire harness plug. Take out three bolts side the shaft and motor out. Replace clutch and install in reverse order.
Parts Used:
Clutch Assembly
  • floyd from Slidell, LA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
23 of 39 people found this instruction helpful.
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All Instructions for the 11088732790
61 - 75 of 1877